ASN Wikibase Occurrence # 376658
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 24 July 1985 |
Time: | 16:45 LT |
Type: | James Gress QUICKIE |
Owner/operator: | Private |
Registration: | N32JG |
MSN: | 0325 |
Total airframe hrs: | 12 hours |
Engine model: | ONAN B48GA018/1A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fenton, MO -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | Fenton, MO (3WE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE TAKING OFF, THE PLT NOTED A PARTIAL LOSS OF ENG POWER DURING THE INITIAL CLIMB. HE WAS UNABLE TO MAINTAIN ALT & TRIED TO MANEUVER AROUND TREES NEAR THE DEPARTURE END OF THE RWY. HOWEVER, THE ACFT DESCENDED INTO THE TREE TOPS, THEN CRASHED ONTO THE ROOF OF A RESIDENTIAL BUILDING. AN EXAM OF THE ENG REVEALED THAT ONE CYLINDER HEAD GASKET WAS LEAKING DURING ENG OPERATION, PROVIDING INSUFFICIENT COMPRESSION TO THAT CYLINDER & A REDUCTION OF POWER. THE ENG HAD ONLY 2 CYLINDERS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC85LA166 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MKC85LA166
Location
Revision history:
Date/time | Contributor | Updates |
29-Mar-2024 18:25 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation