ASN Wikibase Occurrence # 377101
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Date: | Sunday 2 June 1985 |
Time: | 11:00 LT |
Type: | Bellanca 17-30A |
Owner/operator: | Mike Haynes |
Registration: | N39854 |
MSN: | 30483 |
Total airframe hrs: | 1104 hours |
Engine model: | CONTINENTAL IO-520-K |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | El Paso, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | Alamogordo, NM |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER LIFTOFF, THE PLT FIRST SMELLED, THEN OBSERVED SMOKE COMING INTO THE COCKPIT FROM UNDER THE INSTRUMENT PANEL. SHORTLY THEREAFTER, THE ENG QUIT COMPLETELY. THE PLT MADE A FORCED LANDING IN AN OPEN AREA OFF THE RWY. DURING THE LANDING ROLL, THE ACFT STRUCK AN EMBANKMENT & THE LANDING GEAR COLLAPSED. AN INVESTIGATION REVEALED THAT THE MUFFLER ON THE LEFT SIDE, WHICH HAD BEEN OVERHAULED & INSTALLED ON 7/25/83, HAD FAILED NEAR THE OUTLET, ALLOWING HOT EXHAUST GASES TO ENTER THE ENG COMPARTMENT & BURN A WIRE BUNDLE CONTAINING THE MAGNETO WIRING (P-LEADS). A LARGE SECTION WAS MISSING FROM THE REAR HALF OF THE MUFFLER.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW85LA242 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB FTW85LA242
Location
Revision history:
Date/time | Contributor | Updates |
30-Mar-2024 08:15 |
ASN Update Bot |
Added |
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