ASN Wikibase Occurrence # 380066
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 15 February 1984 |
Time: | 18:30 LT |
Type: | Mooney MK20B |
Owner/operator: | Private |
Registration: | N74515 |
MSN: | 1905 |
Year of manufacture: | 1962 |
Total airframe hrs: | 3643 hours |
Engine model: | Lycoming O-360-A1D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Pocahontas, AR -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Pocahontas, AR (M70 |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACFT LANDING GEAR RETRACTED DURING LANDING. THE PLT REPORTED THAT THE MANUALLY ACTIVATED GEAR HANDLE POPPED OUT OF THE GEAR DOWN POSITION DURING THE LANDING ROLL. THE PLT INDICATED THAT HE THOUGHT THE GEAR HANDLE WAS POSITIVELY IN THE DOWN LOCK POSITION.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC84LA082 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MKC84LA082
Location
Revision history:
Date/time | Contributor | Updates |
01-Apr-2024 12:27 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation