ASN Wikibase Occurrence # 380182
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Date: | Monday 23 January 1984 |
Time: | 21:20 LT |
Type: | McDonnell Douglas DC-8-61 |
Owner/operator: | United Airlines |
Registration: | N8081U |
MSN: | 45971 |
Engine model: | GE CF56 |
Fatalities: | Fatalities: 0 / Occupants: 47 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Chicago, IL -
United States of America
|
Phase: | Take off |
Nature: | Unknown |
Departure airport: | Chicago, IL |
Destination airport: | (KYYZ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AS THE CAPT APPLIED POWER & RELEASED BRAKES TO BEGIN THE TAKEOFF, THE ACFT STARTED TO DRIFT TO THE RIGHT. THE CAPT STATED THAT HE CLOSED THE THROTTLES & PUT THE #1 & #2 THROTTLES IN REVERSE. THE ACFT THEN BEGAN TO VEER LEFT & SPUN AROUND NEARLY 1-1/2 TIMES. THE 1ST OFFICER STATED THAT AS THE ACFT INITIALLY DRIFTED TO THE RIGHT, HE NOTED THAT THE #4 ENG WAS NOT SPOOLING UP & HE SO INFORMED THE CAPT. THE RWY CENTERLINE HAD BEEN DEICED & WAS REPORTED WET WITH SCATTERED AREAS OF SNOW; BRAKING ACTION HAD BEEN REPORTED AS GOOD. THE CAPT SAID THAT LIGHT RAIN OR MIST WAS PRESENT AT THE TIME OF THE INCIDENT. THE UNDERSIDE OF THE #3 ENG COWLING WAS GASHED DURING THE INCIDENT & A LANDING LIGHT HAD TO BE REPLACED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI84IA093 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB CHI84IA093
Revision history:
Date/time | Contributor | Updates |
01-Apr-2024 13:44 |
ASN Update Bot |
Added |
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