ASN Wikibase Occurrence # 380270
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 2 January 1984 |
Time: | 02:47 LT |
Type: | Lockheed 1329-25 |
Owner/operator: | Business Jet Airline (bjaa) |
Registration: | N322CS |
MSN: | 5208 |
Total airframe hrs: | 2723 hours |
Engine model: | AIRESEARCH TFE-731-31F |
Fatalities: | Fatalities: 0 / Occupants: 6 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Teterboro, NJ -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Chicago, IL (KPWK) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:N322CS LANDED WITH THE LEFT MAIN LANDING GEAR PARTIALLY EXTENDED AFTER EMERGENCY GEAR EXTENTION PROCEDURES FAILED. INVESTIGATION REVEALED THE LEFT ACTUATOR COVER DOOR & STRUT COVER DOORS JAMMED WHERE THE TWO PASS IN CLOSE PROXIMITY DURING THE GEAR EXTENTION SEQUENCE. THE FAILURE MODE THAT CAUSED THE JAM WAS NOT DETERMINED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC84IA066 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB NYC84IA066
Revision history:
Date/time | Contributor | Updates |
01-Apr-2024 14:42 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation