ASN Wikibase Occurrence # 381367
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Date: | Thursday 21 July 1983 |
Time: | 11:30 LT |
Type: | Cessna 150 |
Owner/operator: | Private |
Registration: | N18188 |
MSN: | |
Total airframe hrs: | 3655 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 0 |
Aircraft damage: | Unknown |
Category: | Accident |
Location: | Johnston, SC -
United States of America
|
Phase: | |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTED THAT BEFORE TAKING OFF, HE PREFLIGHTED THE ACFT & ESTIMATED THAT 6 GAL OF FUEL WAS ON BOARD. ACCORDING TO HIM, THE ENGINE LOST POWER APRX 30 MIN AFTER TAKEOFF & HE WAS UNABLE TO RESTART IT. DURING A FORCED LANDING, HE INTENTIONALLY GROUND LOOPED THE ACFT TO AVOID COLLIDING WITH A FENCE. DURING THE GROUND LOOP, THE NOSE GEAR FAILED. THE ACFT WAS EQUIPPED WITH A 26 GAL FUEL SYS OF WHICH 3.5 GAL WAS UNUSABLE. NORMAL FUEL CONSUMPTION WAS BETWEEN 7.0 & 3.2 GAL/HR. THE PLT REPORTED PROBABLE MISCALCULATION OF FUEL.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL83LA287 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB ATL83LA287
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 02:41 |
ASN Update Bot |
Added |
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