ASN Wikibase Occurrence # 381507
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Date: | Tuesday 5 July 1983 |
Time: | 14:30 LT |
Type: | Cessna 150K |
Owner/operator: | Private |
Registration: | N6056G |
MSN: | 15071556 |
Year of manufacture: | 1969 |
Total airframe hrs: | 5906 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Arcadia, OK -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Antlers, OK (8OF) |
Destination airport: | Guthrie, OK (KGOK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACFT WAS DAMAGED IN A FORCED LANDING AFTER THE ENGINE QUIT FROM FUEL EXHAUSTION. THE PLT HAD MADE AN UNSCHEDULED STOP FOR OIL DURING THE X-COUNTRY FLT. ACCORDING TO THE PLT THE ENGINE BEGAN TO RUN ROUGH WHILE CRUISING AND THEN QUIT COMPLETELY EVEN THOUGH CARBURETOR HEAT WAS USED. A FORCED LANDING FOLLOWED. ACCORDING TO THE POLICE AT THE SCENE THE ACFT WAS EXHAUSTED OF FUEL. THE PLT SAID THE GAUGE READ 1/2 FULL. HE ALSO THOUGHT HE SHOULD HAVE HAD 3 HOURS OF FUEL ANDHAD FLOWN ONLY 2 AND 1/2 HOURS BEFORE POWER LOSS. THE 3 HOURS OF FUEL WAS THE PLTS ESTIMATE OF FUEL ON BOARD AT ORIGINALDEPARTURE.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW83LA316 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB FTW83LA316
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 04:11 |
ASN Update Bot |
Added |
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