ASN Wikibase Occurrence # 381563
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 1 July 1983 |
Time: | 15:00 LT |
Type: | Cessna 172P |
Owner/operator: | Tag Aviation |
Registration: | N62511 |
MSN: | 17275289 |
Year of manufacture: | 1981 |
Total airframe hrs: | 600 hours |
Engine model: | Lycoming O-320-D2J |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Redding, CT -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Block Island, RI (KBID) |
Destination airport: | Spring Valley, NY (N24 |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLIGHT ORIGINATED AT RAMAPO, NY. DURING A PREFLIGHT CHECK, THE PLT NOTED THAT THE FUEL GAUGES INDICATED FULL. WHEN HE VISUALLY CHECKED THE FUEL TANKS, HE ESTIMATED THAT THE FUEL LEVEL IN EACH TANK WAS ABOUT 1 INCH FROM BEING FULL. THE FUEL CAPACITY OF THIS ACFT WAS 54 GAL, OF WHICH, 4 GAL WAS UNUSABLE. THE PLT ESTIMATED THAT HE HAD ENOUGH FUEL FOR THE PLANNED 3 HR FLT. APRX 30 MIN AFTER DEPARTING RAMAPO, HE MADE A PASSENGER STOP AT STORMVILLE, NY. AFTER ANOTHER 1 HR OF FLT, HE LANDED AT BLOCK ISLAND, RI. BEFORE DEPARTING BLOCK ISLAND, HE MADE A PREFLIGHT CHECK & NOTED THAT THE FUEL GAUGES INDICATED SLIGHTLY OVER 1/2 FULL. HOWEVER, HE DID NOT VISUALLY CHECK THE FUEL TANKS BEFORE STARTING THE 1.3 HR RETURN FLT. WHILE EN ROUTE TO SPRING VALLEY, NY, THE ENG LOST POWER AFTER AN ADDITIONAL1 HR OF FLT. DURING A FORCED LANDING, THE ACFT STRUCK BRUSH & SAPLINGS. AFTER THE ORIGINAL DEPARTURE FROM RAMAPO, THE HOBBS METER SHOWED 2.5 HRS ELAPSED TIME. REPORTEDLY, NO FUEL WAS FOUND IN THE TANKS AFTER THE MISHAP.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC83LA161 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB NYC83LA161
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 04:44 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation