ASN Wikibase Occurrence # 382443
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Date: | Friday 11 March 1983 |
Time: | 17:30 LT |
Type: | Rotec RALLY 3 |
Owner/operator: | Robert Boyd |
Registration: | N110RE |
MSN: | 25080 |
Total airframe hrs: | 6 hours |
Engine model: | CUYUNA 430 R |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ultsses, KS -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THIS AMATEUR-BUILT AIRCRAFT WAS BEING FLOWN AT 200 FEET AGL ON A PLEASURE FLIGHT WHEN THE ENGINE QUIT. THE PILOT MADE A FORCED LANDING IN A SOFT FIELD AND THE AIRCRAFT NOSED OVER. THE ENGINE QUIT BECAUSE THE FUEL CAP WAS NOT VENTED. THE CAPWAS SUPPLIED WITH THE KIT BY ROTEX ENGINEERING,INC. AND PRODUCED BY KELCH CORP OF MEGUON,WI, THE CAP WAS LISTED AS VENTED. ON THIS FLIGHT THE PLASTIC FUEL TANK PARTIALLY COLLAPSED DURING THE 20 MINUTE FLIGHT. ALL PREVIOUS FLIGHTS IN THIS AIRCRAFT HAD BEEN OF 15 OR LESS MINUTES WITH NO PROBLEMS IN THE FUEL SYSTEM. THE 4 OWNERS OF THE AIRCRAFT HAD NEVERCHEKCED TO SER IF THE CAP WAS VENTING PROPERLY.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC83LA079 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MKC83LA079
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 13:59 |
ASN Update Bot |
Added |
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