ASN Wikibase Occurrence # 382684
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Date: | Monday 24 January 1983 |
Time: | 10:00 LT |
Type: | Mooney M20K |
Owner/operator: | Private |
Registration: | N97429 |
MSN: | 25-0512 |
Year of manufacture: | 1981 |
Total airframe hrs: | 332 hours |
Engine model: | Continental TSIO-360-GB1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Dufur, OR -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Salem, OK (KSLE) |
Destination airport: | Pasco, WA (KPSC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT COLLIDED WITH AN IRRIGATION PIPE LINE AND FENCE DURING ROLLOUT OF A FORCED LANDING AFTER ENGINE FAILURE. THE ENGINE STOPPED WHILE THE AIRCRAFT WAS CRUISING EN ROUTE. THE PILOT REMAINED IN RADIO CONTACT THROUGHOUT THE EMERGENCY AND LANDED IN A FIELD OF GRAIN STUBBLE AND NEW CROPS. AN ENGINE TEARDOWN REVEALED A HOLE IN THE #4 PISTON. THIS HOLE HAD PRESSURIZED THE CRANKCASE FORCING OIL OUT OF THE BREATHER UNTIL OIL DEPLETION CAUSED ENGINE STOPPAGE. ALSO, A TRACE OF CARBON TRACKING WAS FOUND ON THE RIGHT DISTRIBUTOR BLOCK FROM THE #4 LOCATION TO ANOTHER STATIONARY ELECTRODE.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA83FYM04 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB SEA83FYM04
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 16:29 |
ASN Update Bot |
Added |
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