ASN Wikibase Occurrence # 385226
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 5 December 2022 |
Time: | 18:28 LT |
Type: | Orlican M-8 Eagle |
Owner/operator: | |
Registration: | N602TG |
MSN: | 2022001 |
Year of manufacture: | 2022 |
Total airframe hrs: | 85 hours |
Engine model: | Rotax 912ULS |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | St. Louis, MO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | St. Louis, MO |
Destination airport: | St. Louis, MO |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot and pilot-rated passenger, they performed one traffic pattern takeoff and landing before departing to a practice area with no issues noted while in the traffic pattern. After arriving to the practice area, the pilot initiated a climb and noted a caution indication for the right cylinder head temperature. The pilot reduced engine rpm and descended, and the cylinder temperatures again indicated normal. The pilot added full power to initiate a climb again and he reported that the engine 'stuttered.â The pilot reduced the engine rpm; the engine operated without issue and the pilot added full power again. The pilot reported engine 'stutteredâ again and the stuttering continued when the rpms were reduced. The pilot elected to return to the airport, where the ground visibility was reducing due to dusk light conditions.
The pilot reported that during the return flight to the airport the airplane was struggling to maintain altitude and that he had to fly nose-up to keep from descending. The pilot reported the engine continued to operate in a rough condition. About 20 ft above runway 16, the airplane began to sink, and the pilot added engine power. He stated the engine did not respond, and 'we just fell.â The airplane impacted the runway, veered to the right, and nosed over. The pilot and passenger attempted to secure the airplane's systems and extricated themselves from the airplane.
The recorded flight and engine data revealed no anomalies consistent with what the pilot reported had occurred during the accident flight. Examination of the airframe and engine did not reveal any preimpact mechanical malfunctions or failures that would have precluded normal operation. Based on the evidence and available flight data, it is likely that the pilot failed to fly the airplane at the appropriate airspeed/angle-of-attack during the landing approach, which resulted in an aerodynamic stall and hard landing.
Probable Cause: The pilot's failure to maintain adequate airspeed/angle-of-attack during the landing approach, which resulted in an aerodynamic stall and hard landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN23LA061 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN23LA061
Location
Revision history:
Date/time | Contributor | Updates |
04-Apr-2024 08:04 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation