Accident Piper PA-32RT-300 N3015L,
ASN logo
ASN Wikibase Occurrence # 385412
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 18 August 2001
Time:07:30 LT
Type:Silhouette image of generic P32T model; specific model in this crash may look slightly different    
Piper PA-32RT-300
Owner/operator:Private
Registration: N3015L
MSN: 32R-7985067
Year of manufacture:1979
Total airframe hrs:2520 hours
Engine model:Lycoming IO-540-K1G5D
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Rock Springs, WY -   United States of America
Phase: En route
Nature:Private
Departure airport:Steamboat Sprgs, CO (SBS
Destination airport:Pinedale-Ralph Wenz Field, WY (PWY/KPNA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot was flying the single-engine airplane in cruise flight, when the "aircraft experienced a prop[eller] runaway and loss of oil pressure." The engine began to lose power, so the pilot established the aircraft in a glide toward a dirt road. At 700 feet agl, "a connecting rod poked through the cowling and oil covered the windshield." Due to reduced vision and the unknown condition of the roadway, the pilot elected to make a landing gear retracted landing. The airplane came to rest upright on the shoulder of the road. Examination of the engine revealed that there was no oil present in the engine. The oil filter converter plate gasket was found protruding from around the adapter plate, and a 1/4-inch section of the gasket was missing. An Airworthiness Directive (AD) was issued that addressed the oil filter converter plate gasket on engines that had been factory overhauled after April 1, 1999. The AD required the replacement of the oil filter converter plate gasket before further flight on engines with more than 50 hours time since new, time since overhaul, or time since the last replacement of the gasket or converter plate, and thereafter every 50 hours time in service since the last replacement of the gasket. Non compliance with the AD could result in the protruding or swelling of the converter plate gasket and subsequent loss of engine oil. The engine had been factory overhauled and shipped from the factory on February 18, 2000. At the time of the accident, the engine had accumulated 425 hours since the overhaul. Examination of the engine maintenance records revealed that the AD had not been previously complied with.

Probable Cause: the mechanic's failure to perform an airworthiness directive, which resulted in the loss of engine oil through a partially failed oil filter converter plate gasket, and subsequent failure of a connecting rod during cruise flight. A contributing factor was the lack of suitable terrain for the ensuing forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN01LA149
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB DEN01LA149

History of this aircraft

Other occurrences involving this aircraft
7 April 2005 N3015L Ten Hi Flyers Inc. 1 Broomfield, CO w/o

Location

Revision history:

Date/timeContributorUpdates
04-Apr-2024 18:20 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org