Accident Pitts Special SC-1 N8351,
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ASN Wikibase Occurrence # 385425
 
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Date:Wednesday 15 August 2001
Time:17:30 LT
Type:Silhouette image of generic PTS1 model; specific model in this crash may look slightly different    
Pitts Special SC-1
Owner/operator:
Registration: N8351
MSN: 314F210
Year of manufacture:1972
Total airframe hrs:585 hours
Engine model:Lycoming O-320-E2D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Jerome, ID -   United States of America
Phase: Landing
Nature:Private
Departure airport:Rigby, ID (U56)
Destination airport:Jerome County Airport, ID (KJER)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot, who had just bought the airplane, reported that after a "perfect" three-point landing, the aircraft began a slow drift to the right. He reported that he applied left rudder pedal to counteract the right drift, with no response. He stated that he then added more left rudder, still with no response. The pilot reported that he then applied left brake, but did not get any braking action. The aircraft subsequently departed the runway at a speed estimated by the pilot at about 35 MPH. The left main landing gear then hit a hole and the aircraft came to rest, nose down, about 25 feet off the right side of the runway near the runway exit point. A post-accident inspection disclosed that the left rudder could deflect about 50 to 55 degrees, with maximum right rudder deflection measured at 30 degrees. Full design rudder travel is 30 degrees in either direction. With the rudder at 50 to 55 degrees, the rudder pedal rests against the firewall, preventing the left brake from being applied. The pilot reported that the aircraft received an annual inspection by the previous owner (a certificated airframe and powerplant mechanic) on the date of sale, in July 2001. Follow-up interviews with the previous owner/mechanic and the accident pilot disclosed that the previous owner/mechanic was aware of an anomaly which prevented braking from being applied with rudder pedal deflected at the time he performed the annual inspection, and that he informed the pilot of this anomaly on the day the sale took place.

Probable Cause: The pilot's failure to maintain directional control during landing. Factors included: an incorrectly manufactured or adjusted rudder travel setting, resulting in restricted movement of the left brake; the mechanic's failure to adjust the rudder travel to the correct tolerance; and the pilot's operation of the aircraft with a known equipment deficiency.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA01LA151
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB SEA01LA151

Location

Revision history:

Date/timeContributorUpdates
04-Apr-2024 18:27 ASN Update Bot Added

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