ASN Wikibase Occurrence # 38558
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Date: | Friday 22 October 1999 |
Time: | 15:07 LT |
Type: | Bede BD-5B |
Owner/operator: | Clarence S. Folsom, Jr. |
Registration: | N62765 |
MSN: | 4425 |
Total airframe hrs: | 70 hours |
Engine model: | SOLAR T62T-2A1 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Boulder City, NV -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | , NV (61B) |
Destination airport: | (61B) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the amateur-built airplane took off and entered the traffic pattern. A witness heard the pilot announce his position in the pattern. About 10 seconds later, while the airplane was maintaining a level flight cruise attitude, the airplane began descending, and it turned toward the runway. The witness further reported that the airplane's descent rate increased and the pilot broadcast, "I've got a problem." The airplane appeared to descend at a 30- to 40-degree nose down angle. It impacted a berm about 1 mile short of the landing threshold. This was the first flight following the pilot's installation of the new propeller assembly. Prior to taking off, a witness observed the pilot make a wiring change to the propeller's pitch control electric drive motor. The change was intended to reduce the time necessary to vary the pitch through its full range of travel from 15 to between 7 and 8 seconds. The on-scene examination of the assembly revealed that the wire was disconnected, and the blade pitch was found about the 2-degree (flat blade) position, which would produce considerable drag in flight. No internal malfunctions to the propeller assembly were noted. The pilot, a retired airline captain, was not the builder of the airplane. He did not possess either a repairman or a FAA Airframe & Powerplant certificate.
Probable Cause: The pilot's failure to secure an electrical wire terminal in the propeller pitch control circuit following a maintenance adjustment, which resulted in the propeller malfunctioning and going to a flat pitch. The flat pitch of the propeller produced a high drag which precluded the aircraft from maintaining flight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX00LA023 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX00LA023
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:40 |
ASN Update Bot |
Updated [Operator, Departure airport, Destination airport, Source, Narrative] |
07-Apr-2024 17:17 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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