ASN Wikibase Occurrence # 385705
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Date: | Monday 25 June 2001 |
Time: | 09:20 LT |
Type: | Cessna 172M |
Owner/operator: | Airline Transport Professionals Corp. Of Usa |
Registration: | N1409V |
MSN: | 17263554 |
Year of manufacture: | 1974 |
Total airframe hrs: | 5059 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Napa, CA -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Sacramento-Executive Airport, CA (SAC/KSAC) |
Destination airport: | Napa County Airport, CA (APC/KAPC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the missed approach the engine lost power, was maneuvered to land, and came to rest inverted after the nose wheel touched down in soft dirt. The purpose of the flight was to conduct instrument training at local area airports. The flight had departed home base approximately an hour away from the accident airport. No discrepancies were noted with the engine during the flight or the approach to land. As the student reached MDA the CFI instructed the student to conduct the missed approach. They climbed straight ahead to 500 feet msl and initiated a left-hand turn for compliance with the missed approach procedure. The engine began to lose power. The CFI declared an emergency and conducted the emergency checklist. She turned towards the runway and slipped the airplane down land on the runway. Due to the altitude, she knew they would not make the runway, so she attempted to land in a grassy area past the departure end of the runway. Again, the airplane was too high for landing and she had to maneuver to avoid the airport perimeter fence. The CFI turned away from the fence. When she returned the airplane to wings level flight the wheels touched down. The nose wheel dug into the soft dirt and the airplane flipped over. Examination of the engine revealed that the exhaust push rod housing and exhaust push rod were bent. The crankshaft was manually rotated establishing valve training continuity. No further discrepancies were noted with the engine.
Probable Cause: Loss of engine power due to the restricted movement of the number 1 exhaust valve that subsequently bent the exhaust push rod and push rod housing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX01LA221 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX01LA221
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 07:03 |
ASN Update Bot |
Added |
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