ASN Wikibase Occurrence # 385740
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Date: | Sunday 17 June 2001 |
Time: | 14:00 LT |
Type: | Cessna 150L |
Owner/operator: | Associated Air Activities, Inc. |
Registration: | N6557G |
MSN: | 72057 |
Total airframe hrs: | 5029 hours |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Munster, IN -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Munster, IN |
Destination airport: | Chicago-Lansing Municipal Airport, IL (KIGQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On the previous flight, the airplane experienced a loss of engine power during cruise flight. The airplane was successfully forced landed in the soybean field by another pilot. The owner/accident pilot said that when he arrived at the field, he and one of his line service employees removed the airplane's cowling and "examined [the] control cables, etc." They checked the fuel at both of the fuel tank drains and the main sump. They also did a visual check of the fuel in the tanks. They started the engine with the cowling off and did an engine run up. The owner/pilot shut the engine down, replaced the cowling, restarted the engine, and taxied the airplane to the east edge of the field. The owner/pilot said, "I proceeded to do another run up with mags checking good. I lowered flaps to 20 degrees and started a take off roll to the west." He said that the ground roll and climb out seemed normal and the engine sounded okay. The owner/pilot said that at about 50 to 75 feet above the ground the engine quit. "I pumped the throttle a few times to no avail. With an 8 foot [high] cyclone fence ahead of me, I decided to turn 90 degrees to the left." The owner/pilot said that about the same time the airplane was "making ground contact nose heavy and flipped over on the aircraft's back." The owner/pilot said that he suspected water contamination. He said that they had this problem before with this airplane. The airplane had been tied outside for a couple of weeks, and that they had experienced some heavy rain during that time. An examination of the airplane revealed water in the fuel.
Probable Cause: Engine failure during takeoff due to water contaminating the fuel, the pilot's inadequate preflight planning/preparation, and the low altitude. Factors relating to this accident were the attempted emergency landing after takeoff and the fence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI01LA170 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB CHI01LA170
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 07:23 |
ASN Update Bot |
Added |
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