Serious incident Boeing 727-233 N277FE,
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ASN Wikibase Occurrence # 385867
 
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Date:Friday 25 May 2001
Time:06:24 LT
Type:Silhouette image of generic B722 model; specific model in this crash may look slightly different    
Boeing 727-233
Owner/operator:Federal Express Corp
Registration: N277FE
MSN: 22042/1630
Year of manufacture:1980
Total airframe hrs:33964 hours
Engine model:P&W JT8D-15
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Minor
Category:Serious incident
Location:Harrisburg, PA -   United States of America
Phase: Standing
Nature:Unknown
Departure airport:Memphis International Airport, TN (MEM/KMEM)
Destination airport:Harrisburg International Airport, PA (MDT/KMDT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While a mechanic was performing a "Predispatch Ops Check" on the airplane from the cockpit, ground personnel notified him that smoke was observed coming from the aft stairwell. Fire extinguishing agents were applied to the area and the fire was contained. Examination of the airplane after the incident revealed that the insulation on a wire to the standby hydraulic system electric motor pump had chafed through, allowing the wire conductor to contact a hydraulic system "A" case drain return line. Approximately four feet above the hydraulic line, a 1-inch by 3/16 inch hole was observed in the backside of a reservoir pressurization line, which was fed by a 13th stage bleed-air line. According to Equipment Quality Analysis Reports submitted by Boeing, the chafing between the standby hydraulic pump electrical power wire, and the hydraulic system "A" case drain return line, exposed the standby pump conductor wire and resulted in electrical arcing/puncture to the system "A" return line, followed by ignition to the mist of hydraulic oil leaking from the hole in the line. The wire bundle/tube chafing condition appeared to have occurred from inadvertent mis-routing of the wire bundle during maintenance activity.

Probable Cause: The inadvertent misrouting of a wire harness by maintenance personnel, which resulted in chafing to a hydraulic line and electrical wire, and subsequent fire.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC01IA134
Status: Investigation completed
Duration: 2 years 1 month
Download report: Final report

Sources:

NTSB NYC01IA134

History of this aircraft

Other occurrences involving this aircraft
20 November 2001 N277FE FedEx 0 Memphis, Tennessee sub
Bird strike

Location

Revision history:

Date/timeContributorUpdates
05-Apr-2024 08:45 ASN Update Bot Added

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