Accident Piper PA-32R-300 N40066,
ASN logo
ASN Wikibase Occurrence # 385998
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Sunday 22 April 2001
Time:17:30 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-300
Owner/operator:Private
Registration: N40066
MSN: 7780514
Total airframe hrs:2780 hours
Engine model:Lycoming IO-540-K1G50
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:King George, VA -   United States of America
Phase: En route
Nature:Private
Departure airport:Charlottesville-Albemarle Airport, VA (CHO/KCHO)
Destination airport:Georgetown-Sussex County Airport, DE (GED/KGED)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was in cruise flight at 3,500 feet in the vicinity of the Potomac River when the airplane experienced a partial loss of engine power. The pilot said he checked the magnetos and engine controls, and experienced a slight restoration of power when he adjusted the mixture. Within 3 minutes, there was a total loss of engine power. The pilot turned away from the river, and performed a forced landing to a farm pasture. Examination of the airplane at the scene revealed that the # 3 cylinder was loose on the crankcase, and the number 3 intake tube was not installed, and rested in the bottom of the engine compartment. The #3 exhaust riser was found separated at the flange. The flange was found loose, as the two nuts were not tight, with one nut having no washer or lock washer installed. Further examination revealed the 2 case studs and 2 thru studs along the bottom of the # 3 cylinder were broken off. The cylinder was removed and visually examined. The cylinder skirt exhibited chafing and scratching. There was corresponding scratching to the cylinder case pad material. Examination of the fractured cylinder studs revealed fracture surfaces with features consistent with fatigue. The engine was overhauled 14 years and 917 flight hours prior to the accident, and no cylinders had been removed during that time. The engine manufacturer recommended that the engine be overhauled every 2,000 hours or 12 years, whichever occurred first.

Probable Cause: The failure of cylinder case and thru studs due to fatigue, which resulted in a loss of engine power over unsuitable terrain.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: IAD01LA046
Status: Investigation completed
Duration: 2 years
Download report: Final report

Sources:

NTSB IAD01LA046

Location

Revision history:

Date/timeContributorUpdates
05-Apr-2024 10:02 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org