ASN Wikibase Occurrence # 386199
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Date: | Monday 19 February 2001 |
Time: | 13:10 LT |
Type: | Landry Gyrobee |
Owner/operator: | Private |
Registration: | N392JL |
MSN: | JAL01 |
Total airframe hrs: | 15 hours |
Engine model: | Rotax 503DCDI |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chehalis, WA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Chehalis-Centralia Airport, WA (CLS/KCLS) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that about half way down the runway, he increased power to initiate a "crow-hop" maneuver. As the gyroplane started to become airborne it also began a right drift, which the pilot believed was from a left crosswind with slightly gusty wind conditions. The pilot reported that he "...adjusted the cyclic control to arrest the right drift..," that "...as the aircraft left the surface of the runway and became airborne, it immediately banked and drifted to the right...," and "...in attempting to adjust the cyclic control to level the aircraft, I either failed to move the control adequately, or I mistakenly moved it in the wrong direction...." The pilot reported a total of 918 hours of flight experience (all in rotorcraft) and 15 hours in the accident make. He also reported that "...the accident aircraft was fitted with an overhead cyclic control stick connected directly to the rotor head assembly..." and that "...this type of direct cyclic control can be described as having "reverse" control movements when compared to conventional cyclic control systems..." (e.g., to move the gyroplane right the pilot applies left cyclic). The majority of the pilot's flight experience was in "conventionally" controlled rotorcraft and he believed that he "...may have reverted back to [the] deeply imbedded control reflexes and moved the cyclic control in the wrong direction...."
Probable Cause: The pilot-in-command's reverse application of cyclic to counteract a right drift during the takeoff roll in a gyroplane whose controls had been designed reverse of standard. Contributing factors were the gusty wind conditions and the pilot's "expectancy" or reversion to habit patterns based on non-reversed controls from the majority of his flight experience.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA01LA051 |
Status: | Investigation completed |
Duration: | 1 year and 11 months |
Download report: | Final report |
|
Sources:
NTSB SEA01LA051
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 12:11 |
ASN Update Bot |
Added |
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