ASN Wikibase Occurrence # 386269
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 28 January 2001 |
Time: | 16:41 LT |
Type: | Cessna 182R |
Owner/operator: | Boeing Employees Flying Association |
Registration: | N7568T |
MSN: | R1820039 |
Total airframe hrs: | 5716 hours |
Engine model: | Lycoming O-540-J3C5D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Renton, WA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Olympia Airport, WA (OLM/KOLM) |
Destination airport: | Renton Airport, WA (RNT/KRNT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed Olympia in the Cessna 182R en route to Renton, Washington. Shortly after departure he smelled a "faint odor of electrical insulation" but observed no anomalies. Upon arrival at Renton, he lowered the landing gear, and during the landing roll the main landing gear collapsed. Post-crash examination of the aircraft revealed that the hydraulic power pack had worn gears within the pump assembly. This condition would allow the electrically driven pump to operate for longer than normal periods of time and ultimately resulted in the pump overheating and its associated circuit breaker tripping during the flight. Additionally, the green landing gear "down and locked" annunciator light's manual iris was found to be open only 1/16 of an inch. With the iris stopped down to near total closure the pilot would have been unable to see the green light had it been illuminated. With the electrically driven pump out of service due to the tripped circuit breaker, the gear would not have hydraulic pressure to lock into the down position and complete the circuit thus illuminating the green light, and the pilot failed to verify a down an locked condition other than placing the gear handle in the down position.
Probable Cause: The worn condition of the hydraulic pump gears which resulted in a continuous running pump, subsequent pump motor overheat and eventually the tripping of the pump motor circuit breaker. An additional cause was the pilot's failure to verify that the landing gear were down and locked. A contributing factor was a partially blocked green annunciator light.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA01LA042 |
Status: | Investigation completed |
Duration: | 2 years and 7 months |
Download report: | Final report |
|
Sources:
NTSB SEA01LA042
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 13:04 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation