ASN Wikibase Occurrence # 38672
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Date: | Wednesday 12 February 1992 |
Time: | 13:40 LT |
Type: | Bell 206L-3 LongRanger III |
Owner/operator: | Kusa Television |
Registration: | N99TV |
MSN: | 51280 |
Year of manufacture: | 1989 |
Total airframe hrs: | 1295 hours |
Engine model: | ALLISON 250-C30P |
Fatalities: | Fatalities: 2 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Horsetooth Reservoir, Fort Collins, Colorado -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Denver, CO (KDEN) |
Destination airport: | Fort Collins, CO (3V5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HELICOPTER WAS BEING FLOWN TO A MAINTENANCE FACILITY TO CORRECT A 'ROTOR VIBRATION' THAT HAD BEEN DETECTED BY THE PILOT. WHILE IN CRUISE FLIGHT OVER A RESERVOIR, A LOSS OF ENGINE POWER OCCURRED, WHEN THE #2-1/2 BEARING FAILED DUE TO OIL STARVATION. THE OIL STARVATION RESULTED FROM AN OBSTRUCTION IN THE BEARING OIL FEED TUBE BY A PARTICLE OF FOREIGN MATERIAL. THERE WAS EVIDENCE THE MATERIAL WAS INTRODUCED INTO THE SYSTEM DURING OVERHAUL, ABOUT 9 FLIGHT HOURS BEFORE THE ACCIDENT. THE PILOT MADE AN AUTOROTATION THROUGH DENSE FOG TO THE SURFACE OF THE RESERVOIR, WHICH CONTAINED PATCHES OF ICE. THE HELICOPTER SANK IN 190 FT OF WATER. WATER TEMPERATURE WAS 30 DEG F, AIR TEMPERATURE WAS 34 DEG, AND WIND WAS 170 DEG AT 8 KTS. ACCORDING TO AVAILABLE INFORMATION, USEFUL CONSCIOUS TIME UNDER THESE CONDITIONS WOULD HAVE BEEN ABOUT 15 MIN. THE FIRST RESCUE PERSONNEL REACHED THE PILOT APPROXIMATELY 45 MIN FOLLOWING THE ACCIDENT. THE PILOT WAS THE ONLY PERSON ON THE SURFACE AT THAT TIME.
Probable Cause: FAILURE OF THE NUMBER 2-1/2 BEARING DUE TO AN OBSTRUCTION OF A BEARING OIL FEED TUBE BY FOREIGN MATERIAL. FACTORS RELATED TO THE ACCIDENT WERE: IMPROPER MAINTENANCE DURING ENGINE OVERHAUL, AND WEATHER/TERRAIN/WATER CONDITIONS IN THE EMERGENCY LANDING AREA.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN92FA034 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB DEN92FA034
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=99TV Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
26-Apr-2016 18:05 |
Dr.John Smith |
Updated [Location, Departure airport, Destination airport, Source, Narrative] |
26-Apr-2016 18:06 |
Dr.John Smith |
Updated [Departure airport] |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
11-Apr-2024 09:02 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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