ASN Wikibase Occurrence # 387237
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Date: | Sunday 24 September 2000 |
Time: | 12:45 LT |
Type: | Hughes 269B |
Owner/operator: | Private |
Registration: | N9355F |
MSN: | 44-0073 |
Year of manufacture: | 1964 |
Total airframe hrs: | 2302 hours |
Engine model: | Lycoming HIO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Burlington, WA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Arlington, WA (AWO |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot aborted his landing in the Hughes 269B helicopter after encountering dust and reduced visibility at the landing site. During the climbout, and at 50-60 mph and approximately 140 feet above ground, the engine rapidly lost power. The pilot executed an autorotation landing from an airspeed/altitude condition slightly outside the limitations of the height-velocity diagram and landed hard. Post crash examination revealed that the #1 cylinder fuel injector line had separated approximately one inch outboard of the injector unit. Metallurgical examination revealed the separation as fatigue. The engine log showed this to be the second #1 cylinder fuel injector line separation in recent history. Further examination revealed that 3 of the hold down bolts for the #3 cylinder had separated and metallurgical examination revealed the separations as fatigue. The flange for the #3 cylinder was observed to be painted with primer paint measuring from about 0.0014 inch to 0.0028 inch in thickness. Both cylinder hold down plates were examined and showed fretting and rubbing damage. According to Textron Lycoming Service Bulletin 271A, the primer paint thickness on the flange should not exceed 0.0005 inch. According to the engine log the engine underwent a major overhaul on July 8, 1994, during which the '...engine was painted assembled and delivered to Cascade Airframe Repair....' The #3 cylinder was subsequently removed and honed on an unspecified date. The date when the #3 cylinder flange was painted was not determined.
Probable Cause: Mintenance personnel not following the mandatory service bulletin procedure of not exceeding 0.0005 inch paint thickness on the cylinder flange. Factors were the fatigue separation of multiple cylinder hold down bolts resulting in looseness of the cylinder; and the subsequent vibration and fatigue separation of the fuel injector line. An additional factor was the pilot's operation of the rotorcraft outside the height/velocity parameters for a successful autorotation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA00LA188 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB SEA00LA188
Location
Revision history:
Date/time | Contributor | Updates |
03-May-2024 06:53 |
ASN Update Bot |
Added |
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