ASN Wikibase Occurrence # 387311
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Date: | Saturday 9 September 2000 |
Time: | 13:30 LT |
Type: | Cessna 120 |
Owner/operator: | Private |
Registration: | N76261 |
MSN: | 10666 |
Total airframe hrs: | 3624 hours |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sacramento, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KSAC) |
Destination airport: | Madera, CA (KMAE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the takeoff climb the airplane lost power and collided with the tops of trees during the ensuing emergency landing. The pilot stated there were no mechanical anomalies noted with the preflight, or taxi to the active runway. Prior to takeoff, the airport closed for about 5 minutes. About 4 minutes after the airport reopened, the pilot was cleared for takeoff. After takeoff the engine rpm's dropped. He suspected carburetor icing and applied the carburetor heat. The engine continued to lose power. His intent was to land in-between trees on a golf course. At the last minute he had to maneuver the airplane to avoid a golf cart. He attempted to stall the airplane into the tops of the trees. Witnesses to the accident heard the engine sputtering. At the accident site fuel was found in the left tank, and on the ground underneath the right wing. The airframe and power plant were examined. The fuel selector was stiff to move and the main discharge nozzle was leaking and stained. The carburetor heat control cable retainer bolt washer, and the mixture control cable rod end retainer bolt were both loose. The carburetor was inspected and found in noncompliance with airworthiness directives. No further mechanical anomalies were noted with the airframe, power plant, or carburetor. Conditions at the time of the accident were conducive to carburetor icing.
Probable Cause: The pilot's inadequate preflight planning and his improper use of carburetor heat that resulted in a loss of engine power due to carburetor icing following a delayed takeoff in conditions that were conducive to carburetor icing. A factor was the nonsuitable terrain for landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX00LA332 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX00LA332
Location
Revision history:
Date/time | Contributor | Updates |
03-May-2024 07:44 |
ASN Update Bot |
Added |
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