Accident Piper PA-32R-301 N411JL,
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ASN Wikibase Occurrence # 387439
 
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Date:Friday 18 August 2000
Time:15:30 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-301
Owner/operator:Airwest Inc.
Registration: N411JL
MSN: 32R8213047
Total airframe hrs:3417 hours
Engine model:Lycoming IO-540-K1G5D
Fatalities:Fatalities: / Occupants: 5
Aircraft damage: Substantial
Category:Accident
Location:Kennebunkport, ME -   United States of America
Phase: En route
Nature:Private
Departure airport:Portsmouth, NH (KPSM)
Destination airport:(CYAU)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was in cruise flight at 9,000 feet over the ocean when a loud bang was heard from the engine compartment and the windshield was covered with oil. The pilot said that the engine produced partial power before the engine and propeller stopped. The pilot ditched the airplane in the ocean. Examination of the wreckage revealed there was an 8-inch by 5-inch hole in the top of the engine case. The camshaft was exposed and completely fractured aft of the #3 intake lobe. The #4 connecting rod was fractured about mid point. The upper half of the connecting rod was attached to the piston pin, and the piston was staked in the cylinder. The lower half of the #4 connecting rod and its corresponding bearing cap were not attached to the crankshaft, and were not recovered. The #2 and #6 connecting rods displayed heat damage, while the #4 did not. Metallurgical examination of the recovered portions of the #4 connecting rod revealed failure modes consistent with overstress, but no evidence of a primary failure mode was evident on the recovered components. Examination of the engine maintenance records revealed that the #2 cylinder was removed, repaired, and re-installed 1,020 flight hours prior to the accident.

Probable Cause: Fracture of the #4 connecting rod for undetermined reasons, which resulted in a loss of engine power. A factor was the forced ocean ditching.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: IAD00FA076
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB IAD00FA076

Location

Revision history:

Date/timeContributorUpdates
03-May-2024 08:55 ASN Update Bot Added

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