Bird strike Accident Piper PA-46-310P Malibu N315RC,
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ASN Wikibase Occurrence # 40279
 
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Date:Tuesday 26 June 1990
Time:16:16
Type:Silhouette image of generic PA46 model; specific model in this crash may look slightly different    
Piper PA-46-310P Malibu
Owner/operator:D & M Express
Registration: N315RC
MSN: 46-8508044
Total airframe hrs:710 hours
Engine model:CONTINENTAL TSIO-520-BE
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Lakeville, MI -   United States of America
Phase: En route
Nature:Executive
Departure airport:Flint, MI (FNT)
Destination airport:Akron, OH (CAK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DRG IFR DEP, PLT RCVD PROGRESSIVE ALT CLNCS TO CLIMB TO 15,000'. AT 1607 EDT, HE WAS VCTRD FOR 'A GOOD RATE OF CLIMB' THRU 14,000' WITH CLNC TO PROCEED ON COURSE AFTER LVG 14,000' FOR 15,000'. RADAR DATA INDCD A STEADY CLIMB TIL ACFT WAS ABV 13,000'. AS IT CLIMBED FM 13,300' TO 13,900' (MAX RECORDED ALT), ITS SPD SLOWED FM ABT 115 KTS TO BLO 80 KTS. AT 1613 EDT, PLT WAS CLRD TO PROCD DRCT & CHG FREQ. RADAR DATA SHOWED THAT AFTER RCHG 13,900', ACFT DEVIATED FM COURSE & ENTERED STEEP DSCNT. RADAR CTC WAS LOST & INFLT BREAKUP OCCURRED. PIECES OF WNGS & STABILIZERS WERE FND UP TO 1.5 MI FM FUSELAGE. TRAJECTORY STUDY DISCLOSED BREAKUP OCCURRED BTN 6000' & 9000' MSL. EXAM OF FRACTURES ON MAJOR CMPTS REVEALED CHARACTERISTICS TYPICAL OF OVERSTRESS; NO PREEXISTING CRACKS WERE FND. NO AUTOPLT FAILURE OR BIRD STRIKE WAS FND. CLDS WERE LAYERED TO 20,000'; FRZG LVL WAS ABT 12,500'. THERE WAS EVIDENCE ACFT WAS IN OR NR CONVECTIVE PRECIP ABV FRZG LVL FOR ABT 1.5 MIN BFR RAPID DSCNT. FND PITOT HEAT SW 'OFF' & INDUCTION AIR DOOR IN ITS PRIMARY PSN. (SEE: NTLS/SIR-92/03) CAUSE: THE PILOT'S FAILURE TO USE THE AIRPLANE'S ICE PROTECTION EQUIPMENT, WHICH RESULTED IN A PERFORMANCE LOSS DUE TO INDUCTION ICING, PROPELLER ICING, OR BOTH, WHILE FLYING IN CONVECTIVE INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AT AND ABOVE THE FREEZING LEVEL. THE PERFORMANCE LOSS LED TO A STALL, THE RECOVERY FROM WHICH PROBABLY WAS EXACERBATED BY THE PILOT'S IMPROPER RESPONSE TO ERRONEOUS AIRSPEED INDICATIONS THAT RESULTED FROM BLOCKAGE OF THE PITOT TUBE BY ATMOSPHERIC ICING.

Sources:

NTSB: https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X23371

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-May-2017 10:01 harro Updated [Source]

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