Accident Mooney M20C N6481U, 18 Jan 1992
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ASN Wikibase Occurrence # 40545
 
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Date:18-JAN-1992
Time:17:10
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:private
Registration: N6481U
MSN: 2228
Fatalities:Fatalities: 2 / Occupants: 2
Other fatalities:0
Aircraft damage: Written off (damaged beyond repair)
Category:Accident
Location:Santa Monica, CA -   United States of America
Phase: Take off
Nature:Private
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE 107 HR PVT PLT & PSGR DEPD THE airport FOR AN UNKNOWN DESTN. THE RECENTLY PURCHASED ACFT HADN'T FLOWN FOR SVRL MONTHS. THE ACFT HAD BEEN PARKED OUTSIDE & 5.5' OF RAIN HAD FALLEN IN THE LAST 41 DAYS. THE ACFT WAS REFUELED IMMEDIATELY BFR DEPG & THE FUELER SAID THE PLT SAT INSIDE THE ACFT DRG REFUELING, READING A MAP. THE REFUELER DIDN'T SEE THE PLT MAKE A PREFLT INSPN. HE ALSO NOTED THE ACFT WAS VERY DIRTY. THE FUEL FILLER CAPS WERE OF THE THERMOS CAP STYLE, RECESSED INTO WELLS IN THE WING SFC. FAA SDR'S NOTED 20 INSTANCES OF WATER CONTAMINATION OF FUEL IN THIS MODEL ACFT DRG A PERIOD FROM 1/1/86 TO 9/10/92. OF THE 20 RPRTD INSTANCES, 4 WERE ASSOCIATED WITH LEAKAGE THRU LOOSE FUEL CAPS. DRG THE TAKEOFF & INITIAL CLIMB, THE PLT STATED TO THE TWR THAT 'MY ENGINE KEEPS CUTTING IN AND OUT.' HE WAS CLRD TO LND ON ANY RWY. THE PLT COMPLETED A 180 DEG TURN BACK TWD THE RWY & THE ACFT HIT A PWR POLE OFF THE END & BELOW THE RWY SFC. THE ACFT WAS CONSUMED BY A POST-CRASH FIRE. NO MECH MALFUNCTION/FAILURE WAS FND. SUNSET WAS AT 1712 PST. CAUSE: FUEL CONTAMINATION BY WATER DUE TO THE; 1) FAILURE OF THE FUEL CAPS TO PROPERLY SEAL AGAINST WATER INGESTION, 2) THE PILOTS FAILURE TO ADEQUATELY PERFORM A PREFLIGHT INSPECTION OF THE AIRCRAFT SUFFICIENT TO DETECT THE PRESENCE OF WATER IN THE FUEL TANKS. FACTORS IN THE ACCIDENT WERE THE INADEQUATE FUEL CAP/WELL DESIGN BY THE MANUFACTURER AND THE PILOTS REDUCED ABILITY TO VISUALLY SEE AND AVOID THE POWER POLE DUE TO THE PREVAILING LIGHT CONDITIONS.

Sources:

NTSB: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X14000


Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]

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