ASN Wikibase Occurrence # 40802
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Date: | Friday 10 April 1998 |
Time: | 17:30 LT |
Type: | Hughes 269A |
Owner/operator: | Clark, Ron. A |
Registration: | N5161E |
MSN: | 56-0559 |
Total airframe hrs: | 4730 hours |
Engine model: | Lycoming HIO-360-B1A |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Emmett, ID -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Nampa, ID (S67) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The instructor and the student pilot departed on a training flight with the intention of practicing off airport landings. The instructor maneuvered the helicopter towards a plateau with cliffs on three of its sides, and initiated a demonstration of a pinnacle landing. He then noticed the development of an excessive sink rate and wind change and attempted to correct with collective and throttle. Shortly thereafter, he reached the stop on the throttle and the RPM began decaying. The instructor lowered collective and the rotorcraft impacted the ground hard bouncing back into the air 10-12 feet before striking the ground a second time, during which the tail rotor impacted the ground. Directional control was lost and the rotorcraft rolled over the edge of the plateau and down a steeply sloped embankment. The instructor pilot had logged only 3 hours of flight time, all in the accident aircraft make within the previous 90 days. A weather observation recorded at the Caldwell airport 11 nm south of the accident site reported winds from 110 degrees at 9 knots with gusts to 14 knots. The instructor pilot reported that there was no mechanical malfunction with the rotorcraft during the flight.
Probable Cause: The instructor pilot's failure to maintain the proper rate of descent on landing. Factors were a sudden wind shift, the instructor pilot's lack of recent experience, and terrain drop-off.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA98LA063 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB SEA98LA063
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Apr-2024 13:48 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report] |
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