ASN Wikibase Occurrence # 41127
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Date: | Saturday 16 October 1999 |
Time: | 12:32 LT |
Type: | Rand Robinson KR-2 |
Owner/operator: | Leigh E. Kolka |
Registration: | N85ES |
MSN: | 6457 |
Engine model: | Revmaster 2100-S |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bell Buckle, TN -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Murfreesboro, TN |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Five gallons of fuel were added before the flight departed; after departure the flight proceeded to an airport located approximately 19 nautical miles away where a touch-and-go landing was observed. While flying northbound, northeast of the airport, witnesses heard the engine 'spittering and sputtering.' The airplane was then observed to turn to the left, followed by hearing the engine quit. They then observed the airplane in a nose low attitude, spinning and lost sight due to obstructions. Examination of the accident site by FAA inspectors revealed that the airplane descended vertical with little forward movement. A slight odor of fuel was noted in the damaged fuel tank, but no fuel was found; and no evidence of hydraulic action of the fuel tank was noted. No evidence of flight control preimpact failure or malfunction was noted. A seatbelt was not available for the right seat occupant, and replacement of the retractable main landing gear with a fixed type gear was performed but new weight and balance sheet was not located and the work performed was not documented in the aircraft maintenance records. Weight calculations performed indicate that the airplane was approximately 3 pounds over maximum design gross weight at the time of the accident.
Probable Cause: The poor in-flight planning decision by the pilot-in-command for continuing the flight with inadequate fuel supply and the inadvertent stall by the pilot-in-command following total loss of engine power due to fuel exhaustion. Findings in the accident were the pilot's intentional operation of the airplane with a passenger without providing a restraint system to that person, and operation of the airplane in an over gross weight condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA00LA008 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB MIA00LA008
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:41 |
ASN Update Bot |
Updated [Operator, Destination airport, Source, Narrative] |
07-Apr-2024 17:18 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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