Accident Rans S-12 N410ZE,
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ASN Wikibase Occurrence # 41237
 
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Date:Sunday 4 July 1993
Time:15:53 LT
Type:Silhouette image of generic RS12 model; specific model in this crash may look slightly different    
Rans S-12
Owner/operator:Bish, Gregory Keith
Registration: N410ZE
MSN: 0591083
Engine model:ROTAX 582
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Samoa, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Eureka, CA (033)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
SEVERAL WITNESSES REPORTED THAT THE AIRPLANE, WHICH HAS A REAR MOUNTED ENGINE, SEEMED TO BE HAVING SOME DIFFICULTY WITH CONTROLLABILITY DUE TO THE HIGH WINDS IN THE AREA. THE CONSENSUS WAS THAT THE AIRPLANE APPEARED TO ENTER A STALL, AND THEN IT SPUN SEVERAL TIMES BEFORE IMPACTING THE GROUND. THE AIRCRAFT BALLISTIC PARACHUTE SYSTEM WAS MANUALLY DEPLOYED BY THE PILOT, BUT DID NOT INFLATE BEHIND THE AIRPLANE. THE PARACHUTE WAS FOUND ENTANGLED IN THE CRANKSHAFT JUST FORWARD OF THE PROPELLER. THE PARACHUTE OWNERS MANUAL STATES THE ENGINE SHOULD BE STOPPED PRIOR TO DEPLOYMENT OF THE PARACHUTE. IT ALSO RECOMMENDS NOT DEPLOYING THE PARACHUTE IN 'STRONG WINDS OR CONVECTION', ALTHOUGH NO SPECIFIC GUIDELINES WERE FOUND FOR THE PILOT TO FOLLOW IN THE EVENT HE ENCOUNTERED SUCH PHENOMENA. A SENIOR TECHNICIAN WHO WORKED AT THE PARACHUTE MANUFACTURER APPROVED THE INSTALLATION OF THE PARACHUTE PER PHOTO DOCUMENTATION, AS REQUIRED BY THE MANUFACTURER. THE COMPANY COULD NOT PROVIDE A WRITTEN RECORD OF THE APPROVAL. THE MANUAL DOES NOT ADDRESS A MINIMUM RECOMMENDED ALTITUDE OR A MINIMUM SPEED FOR THE DEPLOYMENT OF THE PARACHUTE. POST CRASH INVESTIGATION FAILED TO FIND ANY PRE EXISTING FAILURE/MALFUNCTION OF THE PROPELLER OR POWERPLANT.

Probable Cause: THE INADVERTENT STALL OF THE AIRPLANE. FACTORS RELATED TO THIS ACCIDENT WERE: THE EMERGENCY PARACHUTE SYSTEM THAT WAS DEPLOYED BY THE PILOT, THE PARTIAL FAILURE OF THE PARACHUTE SURVIVAL EQUIPMENT TO DEPLOY PROPERLY, AND THE INSUFFICIENT INFORMATION PROVIDED BY THE AIRCRAFT PARACHUTE MANUFACTURER.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX93LA276
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB LAX93LA276

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Apr-2024 12:49 ASN Update Bot Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report]

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