ASN Wikibase Occurrence # 41419
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Date: | Saturday 10 May 1997 |
Time: | 09:00 LT |
Type: | Cessna T188C |
Owner/operator: | Precision Applicators, Inc. |
Registration: | N3152J |
MSN: | T18803610T |
Year of manufacture: | 1980 |
Total airframe hrs: | 3550 hours |
Engine model: | Continental TSIO-520-T |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Mitchell, OR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While the pilot was on the ground surveying area of land that he intended on spraying, the airplane was loaded with a pesticide in preparation for an aerial application flight. The pilot then boarded, started, and taxied the airplane for takeoff with no problems noted. He took off to the east, leveled off between 25 and 50 feet above the ground, commenced a steep bank turn to the left, flew over a target field located adjacent to the airstrip, and continued to bank steeply toward the west. The airplane aerodynamically stalled while in a steep turn and suddenly descended into terrain in a steep nose-down attitude. Most of the witnesses did not perceive any unusual engine noises prior to impact. The airstrip was surrounded by rising terrain. The flaps were in the fully retracted position. An examination of the engine, airframe, and systems did not reveal any evidence of preimpact mechanical deficiencies, except for the seat restrain systems. The shoulder harness belt, which was original equipment, was severely deteriorated and had failed during the impact. No evidence of pilot incapacitation was found.
Probable Cause: The pilot's failure to maintain adequate airspeed while maneuvering, which led to a stall. A factor contributing to the accident was the lack of adequate altitude to effect a successful stall recovery.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA97LA104 |
Status: | Investigation completed |
Duration: | 2 years and 8 months |
Download report: | Final report |
|
Sources:
NTSB SEA97LA104
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 15:32 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report] |
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