ASN Wikibase Occurrence # 42026
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 26 August 1998 |
Time: | 11:30 LT |
Type: | Cessna 172L |
Owner/operator: | Frederick E. Knutzen |
Registration: | N1069M |
MSN: | 17259800 |
Year of manufacture: | 1971 |
Total airframe hrs: | 6058 hours |
Engine model: | Lycoming O-320-D2G |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Anacortes, WA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Mount Vernon, WA |
Destination airport: | Stuart Island, WA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he and his passenger met earlier in the morning at the pilot's residence on a lake. The purpose of the flight was to take aerial photos of property on an island. He said that while en route, the flight encountered a lowering overcast layer. He diverted and landed at a marina. He then step-taxied the aircraft through a pass in the direction of the islands. The weather was still poor when they exited the pass and the pilot beached the aircraft in a cove. The flight remained for a period of time before departing toward the islands. The pilot does not recall all of the events leading up to the accident. A boater who came upon the wreckage shortly after the accident, reported that the weather was a low overcast layer at 400 to 500 feet and visibility was one-quarter to one-half mile. The float-equipped aircraft was positioned on the beach, out of the water, with the nose positioned up against the rock outcropping. Impact damage from the terrain was noted to the left wing tip, right wing leading edge, both front end floats were crushed upward and rearward, the lower left side of the engine cowling was crushed rearward, the propeller and spinner were damaged, and the tail cone was broken just aft of the baggage compartment The boater was asked if the pilot said anything about the accident. The boater stated that the pilot said that 'we were going too fast.' During the investigation, there was no evidence found to indicate a mechanical failure or malfunction.
Probable Cause: Terrain clearance was not maintained. A low ceiling and the pilot's inadequate in-flight planning/decision were factors.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA98FA170 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB SEA98FA170
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
06-Apr-2024 13:59 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation