ASN Wikibase Occurrence # 42164
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Date: | Sunday 15 June 1997 |
Time: | 17:05 LT |
Type: | Cessna 152 |
Owner/operator: | Fort Meade Flying Club |
Registration: | N93908 |
MSN: | 15285570 |
Year of manufacture: | 1982 |
Total airframe hrs: | 6449 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Edgewater, MD -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | , MD (KANP) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to flying club records, the purpose of the flight was to complete an initial aircraft check for the pilot in the Cessna 152. The check was part of new member in-processing. The pilot was re-joining the flying club after a 9 year absence. The pilot had performed 3 previous takeoffs and landings prior to the accident takeoff. One witness described all four takeoffs as 'high performance.' Several witnesses described the accident takeoff in written statements. When the airplane reached an altitude of approximately 100 to 150 feet, they stated the airplane pitched up to an 'extremely' nose high attitude. Four witnesses described the pitch angle as '...well over 45 degrees...', '...45 to 60 degrees...', '...60 to 70 degrees up...', and '...60 degrees at least...'. Two witnesses described the pitch angle of the airplane as if it flew, left to right, across a clock face. Each said the nose was up at the '...one o'clock position.' Two witnesses said the airplane was '...just hanging on the prop.' Each pilot was airline transport rated with a combined flight experience of approximately 8,000 hours. Examination of the airplane did not disclose evidence of mechanical malfunction..
Probable Cause: The pilot's excessive maneuver at a low altitude, and the flight instructor's inadequate supervision of the pilot, which resulted in an inadvertent stall/spin.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC97FA118 |
Status: | Investigation completed |
Duration: | 3 years |
Download report: | Final report |
|
Sources:
NTSB NYC97FA118
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 14:52 |
ASN Update Bot |
Updated [Time, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report] |
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