ASN Wikibase Occurrence # 42792
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Date: | Sunday 22 August 1993 |
Time: | 15:45 |
Type: | Beechcraft F35 Bonanza |
Owner/operator: | Ken Marson Flying Club |
Registration: | N3804B |
MSN: | D-4066 |
Total airframe hrs: | 4996 hours |
Engine model: | CONTINENTAL E-225-8 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Flying W Airport (N14), Medford, NJ -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Flying W Airport, NJ (N14) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On Sunday, August 22, 1993, at 1545 eastern daylight time, a Beech F35, N3804B, piloted by Terrance Chamberlain, was substantially damaged when it struck trees and impacted the ground during a forced landing, near the Flying W Airport, Medford, New Jersey. The pilot and passenger were fatally injured. Visual meteorological conditions prevailed. A flight plan had not been filed for the flight operating under 14 CFR 91.
A FLIGHT INSTRUCTOR, WHO HAD JUST COMPLETED A FLIGHT IN THE AIRPLANE, REPORTED THAT BOTH MAIN FUEL TANKS WERE DOWN TO ONE QUARTER FULL, AND THE AUXILIARY TANK WAS AT THREE QUARTERS FULL. DURING REFUELING, THE PILOT OF THIS FLIGHT HAD ONLY THE LEFT TANK FILLED. THE PILOT AND PASSENGER DEPARTED ON A LOCAL FLIGHT, AND AFTER ABOUT 1 HOUR OF FLYING TIME THE PILOT TRANSMITTED ON UNICOM THAT THE ENGINE HAD LOST POWER. AFTER SEVERAL SECONDS HE TRANSMITTED THAT THE ENGINE HAD REGAINED POWER MOMENTARILY AND THEN QUIT AGAIN. THE PILOT ATTEMPTED A FORCED LANDING TO THE AIRPORT RUNWAY, STRUCK A TREE, NOSED OVER AND IMPACTED SEVERAL OTHER TREES. POST ACCIDENT INVESTIGATION REVEALED THE FUEL SELECTOR WAS ON THE RIGHT TANK. THE RIGHT TANK CONTAINED 9 OUNCES OF FUEL WHILE 12 1/2 GALLONS REMAINED IN THE LEFT TANK AND 7 1/2 GALLONS REMAINED IN THE AUXILIARY. THE ENGINE WAS PLACED ON A TEST STAND WITH ALL ORIGINAL COMPONENTS. THE ENGINE STARTED AND RAN WITH NO NOTICEABLE DEFICIENCIES. THE ELECTRICAL BOOST PUMP ALSO OPERATED WHEN TESTED. THIS WAS THE PILOTS SECOND FLIGHT AS A PIC IN THIS TYPE AND MODEL OF AIRPLANE.
Probable Cause: THE PILOT'S FAILURE TO SELECT A FUEL TANK THAT CONTAINED FUEL, AND PERFORM THE EMERGENCY PROCEDURE TO RESTART THE ENGINE, WHICH RESULTED IN FUEL STARVATION AND THE LOSS OF ENGINE POWER. FACTORS ARE THE PILOT'S LACK OF TOTAL EXPERIENCE AND HIS INADEQUATE INFLIGHT PLANNING.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC93FA169 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X13218 Images:
Photos: NTSB
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Oct-2022 00:26 |
Captain Adam |
Updated [Location, Departure airport, Narrative, Accident report, Photo] |
12-Oct-2022 00:26 |
Captain Adam |
Updated [Photo] |
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