ASN Wikibase Occurrence # 43071
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Date: | Saturday 30 June 1984 |
Time: | 12:00 |
Type: | Beechcraft 35 Bonanza |
Owner/operator: | Thomas J Matatall |
Registration: | N3267V |
MSN: | D-715 |
Year of manufacture: | 1947 |
Total airframe hrs: | 5602 hours |
Engine model: | CONTINENTAL E-185-8 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Albuquerque, NM -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Albuquerque, NM (Q64) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACCORDING TO airport PERSONNEL THE PLT WAS KNOWN TO PERFORM MAINTENANCE ON HIS ACFT. THE PLT WAS NOT A LICENSED A&P. ACCORDING TO WITNESSES, THE ACFT TOOKOFF AND CLIMBED TO APRX 200 TO 250 FT AND THE Engine quit. THE ACFT CLIMBED 'A LITTLE MORE', THEN MADE A LEFT BANK TURN OF APRX 60 TO 70 DEGREES. ONE WITNESS STATED, 'I SAW THE AIRPLANE STALL AND DIVE NOSE DOWN. THE LEFT WING WAS LOW AND THE TRACK APPEARED LIKE A STEEP FORWARD SIDE SLIP.' POST CRASH EXAM OF THE ENG REVEALED THAT THE DRIVE SHAFT PIN IN THE FUEL PUMP WAS WORN TO THE POINT THAT MARGINAL ENGAGEMENT COULD HAVE BEEN EXPECTED RESULTING IN A LOSS OF FUEL PUMP DRIVE. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X39901 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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