Accident Piper PA-20 N2841P,
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ASN Wikibase Occurrence # 43258
 
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Date:Tuesday 29 August 1989
Time:19:45
Type:Silhouette image of generic PA20 model; specific model in this crash may look slightly different    
Piper PA-20
Owner/operator:private
Registration: N2841P
MSN: 22-3138
Engine model:LYCOMING O-360-A4A
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Moose Lake, MN -   United States of America
Phase: En route
Nature:Training
Departure airport:Moose Lake, MN (21Y)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE ACFT (PIPER PA-22, CONVERTED TO A PA-20, IAW STC SA45AM) WAS BEING USED TO PROVIDE A BIENNIAL FLT REVIEW FOR THE OWNER/PLT (CONSIDERED AS PIC ON THIS FLT). DRG FLT, THE RGT WING FOLDED BACK OVER THE FUSELAGE & THE ACFT CRASHED. AN EXAM OF THE WRECKAGE REVEALED THE forward LIFT STRUT FOR THE RGT WING HAD FAILED IN AN AREA OF SEVERE CORROSION. THE FAILUREOCCURRED AT THE LOWER PART OF THE LIFT STRUT NEAR THE FUSELAGE ATTACHMENT POINT. AN EXAM OF THE ANNUAL INSPN CHECKLIST INDCD ALL APPLICABLE AIRWORTHINESS DIRECTIVES (AD'S) WERE COMPLIED WITH AS OF 7/21/89 & THAT THE LIFT STRUTS WERE VISUALLY INSPD AT THE ANNUAL INSPN. THE ACFT LOGBOOK SHOWED THAT AD 77-03-08 (REQUIRING MECHANICAL TESTING OF THE LIFT STRUT FOR EVIDENCE OF CORROSION AT 5 YR INTERVALS) HAD BEEN COMPLIED WITH IN JULY 1988. THE AROMA OF LINSEED OIL WAS NOTED IN ALL LIFT STRUTS, BUT POLYMERIZED LINSEED OIL WAS FOUND IN THE RGT & LEFT REAR STRUTS. INTERNAL CORROSION HAD PERFORATED THE RGT forward LIFT STRUT PRIOR TO ITS FAILURE. CAUSE: SEVERE CORROSION OF THE LOWER FORWARD LIFT STRUT FOR THE RIGHT WING, INADEQUATE INSPECTION OF THE LIFT STRUT BY MAINTENANCE PERSONNEL, AND SUBSEQUENT FAILURE OF THE LIFT STRUT, WHICH RESULTED IN AN OVERLOAD FAILURE (FOLDING BACK) OF THE WING. RELATED FACTORS WERE: INADEQUATE INSPECTION PROCEDURES PROVIDED BY THE MANUFACTURER & INADEQUATE SURVEILLANCE BY THE FAA.

Sources:

NTSB: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X29206

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]

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