ASN Wikibase Occurrence # 43798
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Date: | Saturday 5 May 2007 |
Time: | 11:17 |
Type: | Lee Stevens Sorrell SNS-2 Guppy |
Owner/operator: | Private |
Registration: | unreg. |
MSN: | 79 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Stewartstown, PA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Stewartstown, PA (0P2) |
Destination airport: | Brogue, PA (9W8) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The non-current pilot departed in the unregistered single seat airplane from runway 15, and a witness who was located at a hangar on the airfield reported that when the flight was past the departure end of the runway, the airplane turned onto a right crosswind leg. The airplane appeared to be flying slow, then "...nose down vertical into a spin, impacted vertically." Another witness who was driving on a nearby road reported seeing the airplane "...spiral down into the field." The airplane came to rest with the empennage elevated vertically and slightly twisted to the left. The fuselage was crushed to the instrument panel. Flight control continuity was confirmed for roll, and pitch; impact damage to the area of the rudder pedals precluded confirmation of control continuity for yaw. A total of 2.5 gallons of blue tinted 2 cycle fuel/oil mixture were drained from the 5.0 gallon fuel tank, which was free of contamination. One propeller blade was separated at the propeller hub and shattered, while the remaining blade remained secured inside the propeller hub. Examination of the engine revealed numerous discrepancies. A current weight and balance was not available with the installed engine and propeller, therefore, the exact weight and balance at the time of the accident was not determined. CAUSE: The pilot's failure to maintain airspeed resulting in inadvertent stall. Contributing to the accident was the pilot's lack of experience in the airplane.
Sources:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20070517X00573&key=1 Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
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