Accident Cessna 207A Stationair N9941M,
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ASN Wikibase Occurrence # 43885
 
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Date:Tuesday 9 January 2007
Time:10:35
Type:Silhouette image of generic C207 model; specific model in this crash may look slightly different    
Cessna 207A Stationair
Owner/operator:Air Supply Alaska Inc
Registration: N9941M
MSN: 20700748
Year of manufacture:1982
Total airframe hrs:13774 hours
Engine model:Continental IO-520-F27B
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:off Kenai, AK -   United States of America
Phase: En route
Nature:Cargo
Departure airport:Kenai Airport, AK (ENA/PAEN)
Destination airport:Kokhanok Airstrip, AK (9K2)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On January 9, 2007, about 1035 Alaska Standard time, a wheel-equipped Cessna 207A airplane, N9941M, sustained substantial damage when it ditched in the ocean waters of the Cook Inlet during an emergency forced landing, about 18 miles west of Kenai, Alaska. The airplane was being operated as a visual flight rules (VFR) cross-country nonscheduled cargo flight under Title 14, CFR Part 135, when the accident occurred. The airplane was operated by Air Supply Alaska Inc., Kenai. The commercial certificated pilot, the sole occupant, was not located at the accident scene, and is presumed to have received fatal injuries. At the time of the accident, visual meteorological conditions prevailed over the Cook Inlet. As search operations progressed, the weather conditions deteriorated, and instrument meteorological conditions prevailed over the inlet. VFR company flight following procedures were in effect. The flight originated at the Kenai Airport about 1023, and was en route to Kokhanok, Alaska.

The commercial certificated pilot prepared for a VFR cross-country nonscheduled cargo flight under Title 14, CFR Part 135, by preflighting the wheel-equipped airplane and starting the engine. The airplane had been parked on the airport ramp overnight, with an electric engine heater and an engine cover on. A portion of the flight was over ocean waters to a remote village. After engine start, the pilot contacted the company owner and reported that the engine oil pressure appeared to be low, but within the operating range. The owner and the pilot discussed the possible reasons, such as cold ambient temperatures, which was about -20 degrees F. The pilot then departed, and reported to his company that the engine pressure was good. About 10 minutes later, he declared an emergency and stated he was ditching in the water, about 18 miles west of the departure airport. Retrieved track data from the pilot's GPS showed the airplane's maximum altitude was 1,439 feet msl, while crossing the ocean in an area that was about 22 miles wide. A review of the manufacturer's maximum glide distance chart revealed that from an altitude of about 1,500 feet, the airplane could glide about 2.1 nautical miles. The airplane was located about two hours after the accident, floating nose down next to a segment of pan ice, about 8.8 miles from the initial accident location. The pilot was not recovered with the airplane, and subsequent searches did not locate him. Following recovery of the airplane, examination of the engine revealed a 8 X 5 inch hole in the top of the case, adjacent to the number 2 cylinder. The number 2 connecting rod was broken from its crankshaft journal, and broken from the bottom of the piston. The number 1 connecting rod bearing was missing from its normal position on the crankshaft journal and the rod had evidence of high heat. Evidence of oil starvation and high heat signatures to several crankshaft and connecting rod bearings was found throughout the engine, along with a large amount of fragmented bearing material. The pilot was not wearing any personal flotation equipment, and the expected survival time in the 29 degree F ocean water was about 30 minutes. The company's operations manual does not contain a written policy requiring pilot's to maintain sufficient altitude to reach shore when crossing ocean waters.

Probable Cause: The total loss of engine power during cruise flight due to the disintegration of engine bearings and the fracture of a connecting rod, which resulted in a ditching into ice covered ocean water. Factors contributing to the survivability of the accident were the pilot's improper decision to fly over frigid water without sufficient altitude to reach a suitable landing area, the lack of written policy and procedures by the operator requiring sufficient altitude to reach shore when crossing ocean waters, temperature extremes consisting of sub-zero air and below freezing water temperatures, and the lack of personal flotation/survival equipment.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC07FA013
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

20700748

History of this aircraft

Other occurrences involving this aircraft
3 November 1995 N88BC Mark Air Express 0 Toksook Bay, AK sub

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Aug-2011 13:48 TB Updated [Time, Aircraft type, Nature, Source]
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
23-Feb-2017 17:18 TB Updated [Location, Phase, Source, Narrative]
04-Dec-2017 18:27 ASN Update Bot Updated [Operator, Other fatalities, Source, Narrative]
13-Sep-2022 19:54 Captain Adam Updated [Operator, Other fatalities, Departure airport, Destination airport, Narrative, Accident report, Photo]

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