Accident Beechcraft B95A Travel Air N1703Y,
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ASN Wikibase Occurrence # 44682
 
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Date:Thursday 30 September 2004
Time:16:30
Type:Silhouette image of generic BE95 model; specific model in this crash may look slightly different    
Beechcraft B95A Travel Air
Owner/operator:GNS LLC
Registration: N1703Y
MSN: TD-498
Total airframe hrs:7934 hours
Engine model:Lycoming IO-360-B1A
Fatalities:Fatalities: 3 / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:Burlington Municipal Airport (BUU), Burlington, WI -   United States of America
Phase: Take off
Nature:Private
Departure airport:Burlington Municipal Airport, WI (KBUU)
Destination airport:Westosha Airport, WI (WI10)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On September 30, 2004, about 1630 central daylight time, a Beech B95A, N1703Y, piloted by a commercial pilot, was destroyed when it impacted trees and terrain after takeoff from runway 11 (4,300 feet by 75 feet, asphalt), at the Burlington Municipal Airport (BUU), Burlington, Wisconsin. The 14 CFR Part 91 flight was operating in visual meteorological conditions without a flight plan. All three occupants of the airplane were fatally injured. The flight was originating at the time of the accident and was en route to the Westosha Airport, Wilmont, Wisconsin.

A witness observed the airplane takeoff and then make a right turn that increased in bank angle until the airplane impacted the ground. Examination of the airplane's control system revealed no pre-impact abnormalities. Examination of the left engine revealed no pre-impact abnormalities. An examination and subsequent test run of the right engine revealed that the engine would not operate continuously with the installed fuel servo. A flow test of the fuel servo showed that the fuel flow was not within the manufacturer's specifications. Disassembly of the fuel servo showed that the fuel regulator nuts were loose and not the same as those originally supplied by the manufacturer. The measured drag torque of the regulator nuts was below the manufacturer's minimum specifications. An overhaul tag indicated that the fuel servo had been previously overhauled. A search of the aircraft records for the previous 5 years showed no record of the fuel servo being overhauled.

Probable Cause: The improper maintenance of the fuel servo resulting in a loose adjustment nut and subsequent failure of the fuel injection servo which led to a complete loss of power on the right engine. Other causes were the pilot's failure to obtain or maintain minimum controllable airspeed which resulted in an uncommanded roll and subsequent impact with the ground.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI04FA290
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20041006X01587&key=1

Images:




Photos: NTSB

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:24 ASN Update Bot Updated [Operator, Destination airport, Source, Narrative]

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