ASN Wikibase Occurrence # 45068
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 25 September 2003 |
Time: | 16:45 |
Type: | Cessna 152 |
Owner/operator: | Private |
Registration: | N25787 |
MSN: | 15280784 |
Year of manufacture: | 1977 |
Total airframe hrs: | 4813 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Three Oaks, MI -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Three Oaks, MI |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was destroyed when it impacted trees and terrain after takeoff. A witness stated, "My brother, [the pilot], took off from the airstrip in the back of his property for a short flight to "buzz" us and fly over the house. ... The take-off appeared and sounded normal to my other brother and I standing at the house end of the airstrip watching him go. The plane banked to the right and approximately halfway into the turn the nose of the plane pointed straight down so that for 1/2 a second the entire plane was visible just above the far treeline with top (roof) of the plane and the wingspan facing us squarely. It fell straight down disappearing into the neighboring cornfield followed immediately by a small crash sound and then silence." Weather was: Wind 290 degrees at 9 knots, variable between 250 and 310 degrees; visibility 10 statute miles; sky condition few 3,800 feet; temperature 13 degrees C; dew point 4 degrees C; altimeter 30.07 inches of mercury. An on-scene investigation revealed both wing flaps were found retracted and the flap selector was at zero degrees. Fuel was found in the left wing fuel tank and in the carburetor. The right tank was found ruptured. Control continuity was established from the cockpit controls to each flight control surface and to the engine. The engine produced a thumb compression at each cylinder and both magnetos produced a spark at the end of each spark plug lead as the engine's crankshaft was rotated. The propeller exhibited chordwise scratches on the outboard section of one of its blades. The other blade was found with a forward bend. No anomalies were detected with the airplane and engine.
Probable Cause: The pilot not maintaining adequate airspeed resulting in a stall during takeoff. Contributing factors were the buzzing flight and trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI03FA320 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030929X01614&key=1
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Dec-2017 19:28 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation