ASN Wikibase Occurrence # 45206
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Date: | Tuesday 3 June 2003 |
Time: | 09:42 |
Type: | Cessna 182Q Skylane |
Owner/operator: | Private |
Registration: | N630SW |
MSN: | 18265516 |
Year of manufacture: | 1977 |
Total airframe hrs: | 2224 hours |
Engine model: | Continental O-470-U |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Gettysburg, SD -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Dickinson, ND (DIK) |
Destination airport: | Lawrence, KS (LWC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane, piloted by an instrument rated private pilot, was destroyed on impact with terrain. Instrument meteorological conditions prevailed at the time of the accident. The pilot was fatally injured. No flight plan was on file. A witness stated that he dropped the pilot off at the departure airport for his return flight on June 3, 2003, at about 0730 mountain daylight time. The witness did not see the airplane depart. There was no record of a weather briefing for the accident flight. The flight was reported as missing when it did not return. The pilot had in his possession an expired third class medical certificate with no limitations. His logbook showed an entry for an instrument proficiency check on October 11, 2000, and an entry for a flight review on June 12, 2002. The logbook showed the pilot logged 2.4 hours of actual instrument flight time on October 13, 2000, and logged .4 hours of simulated instrument flight time on June 12, 2002. The airplane had a total time and hobbs time of 2,190.7 hours at that annual inspection. The aircraft impacted terrain nearly vertical. The fuselage was found crushed in an accordion like fashion with the empennage resting on top of the cabin area of the fuselage. The engine was disassembled and the crankshaft was found with a separation on the cheek between the fifth and sixth journals. Engine controls were traced from the cockpit to the engine. Both magnetos produced spark when rotated by hand. The Hobbs meter read 2,224.5 hours on-scene. Flight controls were taken to the coroner's office and were not able to be reviewed on scene. The indicated weather along a direct course was moderate to heavy rain around the time accident. Recorded National Track Analysis Program (NTAP) radar data of a flight in the area the accident site was plotted. The track of the flight was southeast. NTAP data showed that the flight, at 1434:45Z [Zulu], started a climb from a pressure altitude of 5,600 feet to a pressure altitude of 7,700 feet at 1439:33Z. The flight's altitude varied between 7,600 and 7,700 feet of pressure altitude until 1442:09Z. The remaining data points exhibited a pattern in the shape of a descending spiral.
Probable Cause: The pilot not maintaining aircraft control in cruise flight leading to his inadvertent spiral. A factor was the pilot's in-flight encounter with moderate to heavy rain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI03FA141 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030611X00853&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Dec-2017 18:51 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
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