ASN Wikibase Occurrence # 45347
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Date: | Thursday 5 December 2002 |
Time: | 20:40 |
Type: | AAA Aircraft Leasing 192 |
Owner/operator: | Four Winds Aircraft |
Registration: | N192FW |
MSN: | FW02050001 |
Total airframe hrs: | 94 hours |
Engine model: | Lycoming IO-360-A1A |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Miami, FL -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Marathon, FL (MTH) |
Destination airport: | New Smyrna Bch, FL (EVB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The aircraft was en route at night when it made several course changes before air traffic control (ATC) lost radio and radar contact with the flight. Witnesses saw the airplane descend to the ground in a nose-down attitude and collided with a building. The body the pilot, who had occupied the right-front seat, was found some distance from the aircraft. He sustained burns injuries over 25 percent of his body. The impact damage precluded determination of the cause of the fire. During the flight, ATC replied no to the pilots query if other flights were reporting the smell of smoke. The investigation revealed a powered six-movement automotive seat was installed the in the left front position. The seat was powered by three motors of which in their original automotive installation were protected by a 30-amp circuit breaker; however, when installed in the aircraft was changed to a 5-amp breaker. In this installation the failure of the motor resulted in the opening of the breaker. If the breaker did not open, the switch would fail which was preceded by the motor overheating. After the installation there were instances of the circuit breaker tripping when the seat had a "larger" occupant. During the accident flight, the pilot-rated passenger who occupied the seat was 6 feet 3 inches tall and weighed 231 pounds. The possibility existed for one of the motors for the seat to overheat, and ignite the seat cushion.
Probable Cause: The inflight fire of undetermined origin, which resulted in pilot incapacitation, loss of aircraft control and an inflight collision with a building.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA03FA024 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20021211X05593&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Dec-2017 18:03 |
ASN Update Bot |
Updated [Departure airport, Source, Narrative] |
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