Accident AAA Aircraft Leasing 192 N192FW,
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ASN Wikibase Occurrence # 45347
 
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Date:Thursday 5 December 2002
Time:20:40
Type:AAA Aircraft Leasing 192
Owner/operator:Four Winds Aircraft
Registration: N192FW
MSN: FW02050001
Total airframe hrs:94 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Miami, FL -   United States of America
Phase: En route
Nature:Executive
Departure airport:Marathon, FL (MTH)
Destination airport:New Smyrna Bch, FL (EVB)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The aircraft was en route at night when it made several course changes before air traffic control (ATC) lost radio and radar contact with the flight. Witnesses saw the airplane descend to the ground in a nose-down attitude and collided with a building. The body the pilot, who had occupied the right-front seat, was found some distance from the aircraft. He sustained burns injuries over 25 percent of his body. The impact damage precluded determination of the cause of the fire. During the flight, ATC replied no to the pilots query if other flights were reporting the smell of smoke. The investigation revealed a powered six-movement automotive seat was installed the in the left front position. The seat was powered by three motors of which in their original automotive installation were protected by a 30-amp circuit breaker; however, when installed in the aircraft was changed to a 5-amp breaker. In this installation the failure of the motor resulted in the opening of the breaker. If the breaker did not open, the switch would fail which was preceded by the motor overheating. After the installation there were instances of the circuit breaker tripping when the seat had a "larger" occupant. During the accident flight, the pilot-rated passenger who occupied the seat was 6 feet 3 inches tall and weighed 231 pounds. The possibility existed for one of the motors for the seat to overheat, and ignite the seat cushion.


Probable Cause: The inflight fire of undetermined origin, which resulted in pilot incapacitation, loss of aircraft control and an inflight collision with a building.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA03FA024
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20021211X05593&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Dec-2017 18:03 ASN Update Bot Updated [Departure airport, Source, Narrative]

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