ASN Wikibase Occurrence # 45663
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Date: | Thursday 10 January 2002 |
Time: | 10:42 |
Type: | Springer Longbow 150 |
Owner/operator: | Private |
Registration: | N150LB |
MSN: | 1 |
Total airframe hrs: | 23 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oak Hill, FL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Titusville, FL (TIX) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was observed to fly a circling maneuver, and then dive vertically into the ground with the engine running. Forensic toxicology revealed 31 percent carbon monoxide in the pilot's blood. Metallurgical examination of the exhaust muffler and heat exchanger assembly revealed the wall of the muffler was fractured through in the area where the exhaust pipe was welded to the muffler canister. Fracture surfaces darkly colored by corrosion were observed at the edge of the weld bead around the exhaust port over a circumference of approximately 180 degrees, and along several cracks branching outward from the weld bead. Fracture surfaces that displayed no corrosion branched out circumferentially from the corroded fracture surfaces on either end of the exhaust outlet. A review of Federal Aviation Administration Advisory Circular AC65-12A revealed in Chapter 2, Induction and Exhaust Systems, Exhaust System Repairs: "It is generally recommended that exhaust stacks, mufflers, tailpipes, etc., be replaced with new or reconditioned components rather than repaired".
Probable Cause: The improper modification of the exhaust muffler which resulted in fractures that enabled the contamination of the cabin heating and ventilation system. The pilot subsequently became incapacitated by carbon monoxide poisoning, and the airplane descended uncontrolled into terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL02LA035 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20020115X00070&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Dec-2017 15:22 |
ASN Update Bot |
Updated [Source, Narrative] |
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