ASN Wikibase Occurrence # 45805
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Date: | Saturday 21 July 2001 |
Time: | 13:22 |
Type: | Beechcraft K35 Bonanza |
Owner/operator: | Private |
Registration: | N6062E |
MSN: | D-5999 |
Year of manufacture: | 1959 |
Total airframe hrs: | 3972 hours |
Engine model: | Continental IO-470-C(9) |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Grafton, IA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Cherokee, IA (CKP) |
Destination airport: | Oshkosh, WI (OSH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was destroyed when it impacted the terrain in a muddy soybean field. The private pilot was not instrument rated. A witness reported the pilot was concerned about the weather and delayed the takeoff until about 1200. A 1258 special weather observation from a weather station located 20 miles northwest of the accident site, reported winds from 260 degrees at 8 knots gusting to 18 knots, visibility 3/4 miles, ceiling overcast at 200 feet, and lightning distant all quadrants. The 1319 special weather observation reported winds from 070 degrees at 7 knots, visibility 7 miles, scattered clouds at 400 feet, scattered clouds at 1,700 feet, ceiling overcast at 2,300 feet, and lightning distant all quadrants. The National Transportation Safety Board (NTSB) Meteorology Factual report stated, "The general route of flight indicates the flight was operating under light to moderate weather echoes for the majority of the flight, a brief break in the echoes until just prior to encountering intense to extreme echoes in the general vicinity of the accident site." A witness, who was located approximately one mile north of the accident site, reported a heavy downpour of rain (1.0 inch measured), high winds, pea size hail, and lightning between approximately 1315 and 1330. The inspection of the airplane wreckage revealed no preexisting anomalies to the airframe or engine.
Probable Cause: The pilot's improper inflight decision to continue into known adverse weather. A factor was the thunderstorm.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI01FA230 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010727X01533&key=1 Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 11:50 |
ASN Update Bot |
Updated [Departure airport, Source, Narrative] |
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