Serious incident McDonnell Douglas MD-88 N924DL,
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ASN Wikibase Occurrence # 48751
 
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Date:Thursday 11 December 2008
Time:17:12 LT
Type:Silhouette image of generic MD88 model; specific model in this crash may look slightly different    
McDonnell Douglas MD-88
Owner/operator:Delta Air Lines
Registration: N924DL
MSN: 49711
Total airframe hrs:53506 hours
Engine model:Pratt & Whitney JT8D
Fatalities:Fatalities: 0 / Occupants: 153
Aircraft damage: Minor
Category:Serious incident
Location:Greenville-Spartanburg Airport, SC (GSP/KGSP) -   United States of America
Phase: En route
Nature:Passenger - Scheduled
Departure airport:Washington-Dulles International Airport, DC (IAD/KIAD)
Destination airport:Atlanta Hartsfield-Jackson International Airport, GA (ATL/KATL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While cruising at 30,000 feet, the captain and first officer initially smelled smoke in the cockpit, prompting them to initiate an unscheduled, precautionary landing at an airport along their route. While descending, the crew noticed that smoke was “pouring out' from underneath the first officer's glare shield and instrument panel. No fire or flames were present. The captain declared an emergency and proceeded to depressurize the aircraft while descending through 10,000 feet in order to clear the smoke from the cockpit. Four tires on the left main gear burst on touchdown, and the aircraft came to rest on the runway. Ground personnel notified the crew that the right main brake system was on fire, and the crew and passengers made an emergency evacuation from the left side of the aircraft.

The DC Ground Service Tie Relay (R2-51) and Blocking Diode Assemblies (R7-50 and R7-51), located in the forward accessory compartment of the airplane, exhibited signs of overheating and smoke damage. A detailed examination of the components revealed internal damage consistent with arcing of the electrical contacts. However, due to the extent of the damage, the cause of the arcing could not be determined.

Probable Cause: The overheating and arcing of the DC Ground Service Relay and Block Diodes component for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DCA09IA018
Status: Investigation completed
Duration: 2 years and 4 months
Download report: Final report

Sources:

NTSB DCA09IA018
http://www.greenvilleonline.com/article/20081211/NEWS01/81211023/1001/NEWS https://flightaware.com/live/flight/DAL1102/history/20081211/2034Z/KIAD/KGSP

Location

Revision history:

Date/timeContributorUpdates
12-Dec-2008 02:23 relax630 Added
12-Dec-2008 02:26 harro Updated
12-Dec-2008 22:55 relax630 Updated
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]

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