ASN Wikibase Occurrence # 59766
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Date: | Friday 1 May 2009 |
Time: | 15:18 |
Type: | Cessna 182Q Skylane |
Owner/operator: | Private |
Registration: | N382CH |
MSN: | 18267390 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3000 hours |
Engine model: | Teledyne Continental IO-550D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Thun Field Near Tacoma WA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Puyallup, WA (PLU) |
Destination airport: | Bremerton, WA (PWT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the accident flight was the first flight following maintenance that replaced the fuel sending units, which required draining the fuel tanks. The pilot stated that maintenance personnel added 20 gallons of fuel to each main tank following the work. He did not physically check the fuel level in the tanks, but noted that both fuel gages indicated the same amount of fuel prior to flight. He reported that the engine lost power about 500 feet above ground level on takeoff, and he made an off airport landing that damaged the wings, airframe, and rudder. A Federal Aviation Administration (FAA) inspector examined the airplane the night of the accident, and noted that no fuel was in the left main tank, but maintenance personnel drained about 20 gallons from the right tank. On a follow-up exam, investigators added 5 gallons of fuel to the left wing tank. The engine started immediately without hesitation. It accelerated smoothly to 1,800 rpm, and a magneto check revealed no anomalies. The engine was decelerated to idle rpm; the engine ran smoothly, and shutdown was unremarkable. The airplane had a recording engine data management unit installed. Data indicated that fuel flow dropped to 0 gallons per hour 6 seconds prior to a loss of rpm.
Probable Cause: A loss of engine power due to fuel starvation as a result of the pilot’s failure to verify the fuel levels in the tanks, and, his failure to select the proper fuel tank.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR09LA223 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
02-May-2009 05:05 |
CMLynn |
Added |
02-May-2009 23:02 |
Anon. |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 14:52 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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