Fuel exhaustion Accident Cessna 172M Skyhawk N12151,
ASN logo
ASN Wikibase Occurrence # 65308
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 30 May 2009
Time:10:44
Type:Silhouette image of generic C172 model; specific model in this crash may look slightly different    
Cessna 172M Skyhawk
Owner/operator:Private
Registration: N12151
MSN: 17261846
Year of manufacture:1973
Engine model:Lycoming O-320 SERIES
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:3400 block in Old Oak Dr., Sarasota, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Venice, FL (VNC)
Destination airport:Sarasota, FL (SRQ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
About 7 months before the accident, the carburetor was overhauled, but after installation, the engine could not be restarted when it was hot, and lost power one time in flight. The carburetor was returned to the overhaul facility, repaired, and re-installed a second time. According to the pilot-rated co-owner/passenger, the engine ran "fine" during a test flight, and no flights were conducted between the test flight and the accident flight. Estimates by the pilot and passenger indicated that the accident flight departure fuel quantity was between 26 and 32 gallons. The pilot and passenger departed their home airport for another airport approximately 20 miles away, conducted two touch-and-go landings, and began the return leg to their home airport. While in cruise at 1,100 feet, the engine ran roughly for a brief period of time, and then lost all power. The pilot attempted to restart the engine, but was unsuccessful. The airplane struck trees, and came to rest approximately 25 feet above the ground, suspended by the trees. Based on the pilot's account of the departure fuel quantity and the duration of the flight, the airplane manufacturer's fuel consumption rates did not support the case for fuel exhaustion, but neither the pre-flight nor post- accident fuel quantities were able to be accurately determined. The engine was operated successfully in a post-accident ground test, and subsequent examination and test of the carburetor did not reveal any anomalies. When the intersection of the local temperature and dew point values was located on a chart that depicted carburetor ice envelopes, the point was in the envelope entitled "Serious Icing at Glide Power," near the boundary of the envelope entitled "Icing - Glide and Cruise Power."
Probable Cause: A loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA09LA310
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
31-May-2009 10:54 Digitalis Added
16-Jun-2009 03:11 RobertMB Updated
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
02-Dec-2017 14:56 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org