Accident Piper PA-32-260 Cherokee Six N4864S,
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ASN Wikibase Occurrence # 68349
 
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Date:Thursday 24 September 2009
Time:20:44
Type:Silhouette image of generic PA32 model; specific model in this crash may look slightly different    
Piper PA-32-260 Cherokee Six
Owner/operator:Galt Zone LLC
Registration: N4864S
MSN: 32-1288
Year of manufacture:1970
Total airframe hrs:3789 hours
Engine model:Lycoming O-540-E4B5
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Near Oakland-Troy Airport (KVLL), Michigan -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Troy, MI (KVLL)
Destination airport:Hillsdale, MI (KJYM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during his preflight inspection, he verified the fuel quantity and its distribution in the airplane's four fuel tanks. He noted that both inboard (main) fuel tanks were essentially empty and that both outboard (tip) tanks were almost full. He stated that he performed the accident takeoff using fuel from the left tip tank. Before takeoff, he verified that no anomalies existed with the engine operation during the engine check and when he applied power for takeoff. The pilot performed a short-field takeoff with 20 degrees of flaps. The pilot stated that, as the airplane approached the departure end of the runway, the engine experienced a "quick loss of power," which was shortly followed by a sustained loss of power. The pilot immediately performed a forced landing in a parking lot just north of the departure threshold. During the forced landing, the airplane impacted a shopping cart corral and a tree and then slid down an embankment. The right wing tip and tank were sheared off during impact, and a postimpact ground fire ensued at the sheared right wing tip.

Postaccident examination of the airplane revealed that the left tip tank contained 4.5 gallons of fuel, about 1/4 of its 17-gallon capacity. (The pilot stated in a postaccident interview that the left tip tank contained 1/2 to 3/4 of its total capacity.) The left main tank contained about 0.6 gallons of fuel. The right main tank did not contain any fuel; however, the fuel drain for that tank was separated from the tank during impact. No fuel was observed leaking from the right main tank, nor was there an odor of leaking fuel. The right tip tank was destroyed by impact damage and the subsequent fire.

The cockpit fuel selector was found positioned on the left tip tank. During a postaccident interview with a Federal Aviation Administration inspector, the pilot stated that, after the loss of engine power, he reached for the fuel selector but was unsure of what he did because his attention was diverted by the stall warning light.

An operational engine test run revealed no anomalies. The pilot stated that he believed the loss of engine power during initial climb was likely due to fuel starvation, as a result of fuel sloshing in the left tip tank during rotation and initial climb. However, calculations, testing, and operational history showed that the left tip tank would not unport and experience fuel starvation leading to loss of engine power if it contained 4.5 gallons of fuel unless maneuvering during a turning takeoff was extreme. The accident airplane did not experience extreme maneuvers during or immediately after takeoff. Global positioning system (GPS) data downloaded from the pilot's handheld receiver showed that ground maneuvering for the accident takeoff was routine and did not achieve the lateral accelerations necessary to disrupt fuel flow from the left tip tank. Thus, a takeoff using the left tip tank containing 4.5 gallons of fuel would not result in fuel starvation and, ultimately, loss of engine power.

Additional testing showed that if a fuel tank was depleted of its useable fuel, the engine would continue to run at takeoff power for an additional 35 to 40 seconds. GPS data for the accident flight showed that the loss of engine power likely occurred 22 to 27 seconds after the takeoff roll was initiated. A takeoff on an empty or nearly empty main tank could result in fuel starvation. The accident takeoff was likely performed on an empty or nearly empty main tank.

Probable Cause: A loss of engine power during initial climb due to fuel starvation as a result of the pilot's selection of an empty or nearly empty main tank for takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN09LA605
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
27-Sep-2009 07:54 slowkid Added
27-Sep-2009 10:31 slowkid Updated
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
02-Dec-2017 16:17 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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