ASN Wikibase Occurrence # 69457
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 27 October 2009 |
Time: | 08:42 |
Type: | Beechcraft A36TC Bonanza |
Owner/operator: | Private |
Registration: | C-FFIH |
MSN: | EA258 |
Year of manufacture: | 1981 |
Total airframe hrs: | 3167 hours |
Engine model: | Teledyne Continental TSIO-520-UB |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Near Kalamazoo/Battle Creek International Airport (KAZO), Michigan -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Kalamazoo, MI (AZO) |
Destination airport: | Muskoka, ON, (CYQA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Witnesses and global positioning system data indicated that after takeoff the airplane tracked the runway centerline and climbed approximately 150 feet above ground level before turning to the right and descending. The airplane subsequently impacted the ground, a fence, and a pole about 1,400 feet from the departure end of the runway. A postimpact fire ensued. After acknowledging the takeoff clearance, no further communications were received from the accident airplane. Examination of the airplane’s structure, flight controls, engine controls, and fuel system did not reveal any anomalies consistent with a preimpact failure. The engine manufacturer had issued a Mandatory Service Bulletin (MSB) that was applicable to the accident airplane’s engine. The airplane’s engine was disassembled in order to replace components damaged during the impact sequence. During the disassembly the valve lifters that were the subject of the MSB were examined and found to have pitting. However, the engine was reassembled with the original valve lifters for a functional test run and during the test run the engine produced full rated power and no anomalies were noted. Data retrieved from an engine monitoring system installed on the accident airplane recorded a significant reduction in engine power during the accident takeoff. The monitoring system did not record throttle, mixture, or propeller control positions and the data was consistent with normal power reductions recorded during the landing phase of previous flights. No mechanical reason for the loss of engine power was found.
Probable Cause: The loss of engine power for an undetermined reason.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | A09F0151 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
27-Oct-2009 08:48 |
slowkid |
Added |
27-Oct-2009 09:32 |
robbreid |
Updated |
05-Oct-2010 15:34 |
Anon. |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 17:07 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation