ASN Wikibase Occurrence # 70038
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Date: | Tuesday 10 November 2009 |
Time: | 17:35 |
Type: | Beechcraft 35-B33 Debonair |
Owner/operator: | Private |
Registration: | N9617Y |
MSN: | CD-583 |
Total airframe hrs: | 3774 hours |
Engine model: | Teledyne Continental IO-470 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Chico Airport, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Portland-Hillsboro Airport, OR (HIO/KHIO) |
Destination airport: | Chico Airport, CA (CIC/KCIC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, she filled the fuel tanks prior to departure for the cross-country flight. She switched the fuel selector position every 30 minutes during the flight in an effort to alternate between tanks. She switched to the fullest (left) tank while on approach to the airport. The airplane was on a stable glide path with the gear and flaps down, mixture rich, and propeller at low pitch. On final approach, about 100 feet above ground level, the engine experienced a loss of power. Despite the pilot’s efforts, which included switching to the right tank and turning the fuel boost pump to the "on" position, the engine would not restart. The pilot banked to the right to avoid the runway approach lights and the wing tip subsequently struck the ground, about 200 feet from the runway. The airplane tumbled in a cartwheel-type maneuver before coming to a stop in a nose-down attitude.
First responders observed no fuel in the right wing fuel tank and drained about 12.5 gallons of fuel from the left wing fuel tank. During a postaccident examination, with the airplane in a level attitude, investigators drained 10 gallons of fuel from the right fuel tank and found fuel in the gascolator. Investigators discovered no anomalies that would have precluded normal operation of the airframe or engine.
Probable Cause: A loss of engine power during final approach for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA053 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
11-Nov-2009 00:15 |
RobertMB |
Added |
11-Nov-2009 05:35 |
RobertMB |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 17:48 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
20-Sep-2023 09:25 |
Ron Averes |
Updated [[Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]] |
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