ASN Wikibase Occurrence # 76361
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 5 May 1995 |
Time: | 11:55 LT |
Type: | Piaggio P-149D |
Owner/operator: | Warbird Aircraft Restoration |
Registration: | N253FW |
MSN: | 253 |
Engine model: | Lycoming GO-480-B1A6 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near St Augustine Airport, FL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | (KSGJ) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER TAKEOFF WHILE TURNING LEFT CROSSWIND AT 300-400 FEET ABOVE GROUND LEVEL, THE ENGINE QUIT. THE PREVIOUS OWNER WHO WAS DEMONSTRATING THE AIRPLANE TO THE CURRENT OWNER TOOK THE FLIGHT CONTROLS AND MANEUVERED THE AIRPLANE FOR LANDING. DURING THE DESCENT THE AIRPLANE COLLIDED WITH TREES THEN THE GROUND. EXAMINATION OF THE AIRPLANE AT THE ACCIDENT SITE BY AN FAA INSPECTOR REVEALED NO EVIDENCE OF FUEL LEAKAGE BENEATH THE RIGHT WING FUEL TANK WHICH WAS FOUND TO BE IMPACT DAMAGED. EXAMINATION OF THE ENGINE REVEALED NO EVIDENCE OF MECHANICAL FAILURE OR MALFUNCTION. EXAMINATION OF THE ENGINE-DRIVEN FUEL PUMP AND INLET FUEL LINE TO THE PRESSURE CARBURETOR REVEALED ONLY 1 OR 2 DROPS OF FUEL IN EACH COMPONENT. THE FUEL SELECTOR WAS POSITIONED TO THE RIGHT WING FUEL TANK WHICH WAS DETERMINED TO BE THE FULLEST OF THE TWO TANKS BEFORE TAKEOFF. THE ENGINE HAD BEEN OPERATED FOR ABOUT 1 HOUR 25 MINUTES AT THE TIME OF THE ACCIDENT.
Probable Cause: INADEQUATE FUEL MANAGEMENT BY THE PILOT-IN-COMMAND RESULTING IN THE TOTAL LOSS OF ENGINE POWER DUE TO FUEL STARVATION. CONTRIBUTING TO THE ACCIDENT WAS THE UNSUITABLE TERRAIN ENCOUNTERED DURING THE EMERGENCY DESCENT FOR THE FORCED LANDING.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA95LA126 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB MIA95LA126
Location
Revision history:
Date/time | Contributor | Updates |
16-Aug-2010 04:33 |
TB |
Added |
11-Apr-2011 03:28 |
TB |
Updated [Aircraft type, Source] |
13-Apr-2011 14:41 |
TB |
Updated [Departure airport, Source, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 15:24 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation